mirror of https://gitee.com/openkylin/linux.git
ARM: OMAP4: Workaround the OCP synchronisation issue with 32K synctimer.
On OMAP4, recently a synchronisation bug is discovered by hardware team, which leads to incorrect timer value read from 32K sync timer IP when the IP is comming out of idle. The issue is due to the synchronization methodology used in the SYNCTIMER IP. The value of the counter register in 32kHz domain is synchronized to the OCP domain register only at count up event, and if the OCP clock is switched off, the OCP register gets out of synch until the first count up event after the clock is switched back -at the next falling edge of the 32kHz clock. Further investigation revealed that it applies to gptimer1 and watchdog timer2 as well which may run on 32KHz. This patch fixes the issue for all the applicable modules. The BUG has not made it yet to the OMAP errata list and it is applicable to OMAP1/2/3/4/5. OMAP1/2/3 it is taken care indirectly by autodeps. By enabling static depedency of wakeup clockdomain with MPU, as soon as MPU is woken up from lowpower state(idle) or whenever MPU is active, PRCM forces the OCP clock to be running and allow the counter value to be updated properly in the OCP clock domain. The bug is going to fixed in future OMAP versions. Reported-Tested-by: dave.long@linaro.org [dave.long@linaro.org: Reported the oprofile time stamp issue with synctimer and helped to test this patch] Signed-off-by: Santosh Shilimkar <santosh.shilimkar@ti.com> Signed-off-by: Kevin Hilman <khilman@ti.com>
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@ -196,7 +196,7 @@ static void omap_default_idle(void)
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static int __init omap4_pm_init(void)
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{
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int ret;
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struct clockdomain *emif_clkdm, *mpuss_clkdm, *l3_1_clkdm;
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struct clockdomain *emif_clkdm, *mpuss_clkdm, *l3_1_clkdm, *l4wkup;
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struct clockdomain *ducati_clkdm, *l3_2_clkdm, *l4_per_clkdm;
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if (!cpu_is_omap44xx())
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@ -220,14 +220,19 @@ static int __init omap4_pm_init(void)
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* MPUSS -> L4_PER/L3_* and DUCATI -> L3_* doesn't work as
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* expected. The hardware recommendation is to enable static
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* dependencies for these to avoid system lock ups or random crashes.
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* The L4 wakeup depedency is added to workaround the OCP sync hardware
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* BUG with 32K synctimer which lead to incorrect timer value read
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* from the 32K counter. The BUG applies for GPTIMER1 and WDT2 which
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* are part of L4 wakeup clockdomain.
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*/
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mpuss_clkdm = clkdm_lookup("mpuss_clkdm");
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emif_clkdm = clkdm_lookup("l3_emif_clkdm");
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l3_1_clkdm = clkdm_lookup("l3_1_clkdm");
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l3_2_clkdm = clkdm_lookup("l3_2_clkdm");
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l4_per_clkdm = clkdm_lookup("l4_per_clkdm");
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l4wkup = clkdm_lookup("l4_wkup_clkdm");
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ducati_clkdm = clkdm_lookup("ducati_clkdm");
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if ((!mpuss_clkdm) || (!emif_clkdm) || (!l3_1_clkdm) ||
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if ((!mpuss_clkdm) || (!emif_clkdm) || (!l3_1_clkdm) || (!l4wkup) ||
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(!l3_2_clkdm) || (!ducati_clkdm) || (!l4_per_clkdm))
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goto err2;
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@ -235,6 +240,7 @@ static int __init omap4_pm_init(void)
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ret |= clkdm_add_wkdep(mpuss_clkdm, l3_1_clkdm);
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ret |= clkdm_add_wkdep(mpuss_clkdm, l3_2_clkdm);
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ret |= clkdm_add_wkdep(mpuss_clkdm, l4_per_clkdm);
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ret |= clkdm_add_wkdep(mpuss_clkdm, l4wkup);
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ret |= clkdm_add_wkdep(ducati_clkdm, l3_1_clkdm);
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ret |= clkdm_add_wkdep(ducati_clkdm, l3_2_clkdm);
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if (ret) {
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