In present driver, shutdown clears RTS and DTR in CR register. But the
documentation "Documentation/serial/driver" suggests not to disable
RTS and DTR in shutdown(). Also RTS and DTR is preserved between shutdown
and startup calls, i.e. these are restored in startup if they were enabled
while doing shutdown. So that if RTS and DTR are set using pl011_set_mctrl
then it should continue even after shutdown->startup sequence.
For throttling/unthrottling user should call pl011_set_mctrl.
Signed-off-by: Shreshtha Kumar Sahu <shreshthakumar.sahu@stericsson.com>
Acked-by: Linus Walleij <linus.walleij@linaro.org>
Acked-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
It seems that when the transmit FIFO threshold is reached on OMAP
UARTs, it does not result in a PRCM wakeup. This appears to be a
silicon bug. This means that if the MPU powerdomain is in a low-power
state, the MPU will not be awakened to refill the FIFO until the next
interrupt from another device.
The best solution, at least for the short term, would be for the OMAP
serial driver to call a OMAP subarchitecture function to prevent the
MPU powerdomain from entering a low power state while the FIFO has
data to transmit. However, we no longer have a clean way to do this,
since patches that add platform_data function pointers have been
deprecated by the OMAP maintainer. So we attempt to work around this
as well. The workarounds depend on the setting of CONFIG_CPU_IDLE.
When CONFIG_CPU_IDLE=n, the driver will now only transmit one byte at
a time. This causes the transmit FIFO threshold interrupt to stay
active until there is no more data to be sent. Thus, the MPU
powerdomain stays on during transmits. Aside from that energy
consumption penalty, each transmitted byte results in a huge number of
UART interrupts -- about five per byte. This wastes CPU time and is
quite inefficient, but is probably the most expedient workaround in
this case.
When CONFIG_CPU_IDLE=y, there is a slightly more direct workaround:
the PM QoS constraint can be abused to keep the MPU powerdomain on.
This results in a normal number of interrupts, but, similar to the
above workaround, wastes power by preventing the MPU from entering
WFI.
Future patches are planned for the 3.4 merge window to implement more
efficient, but also more disruptive, workarounds to these problems.
DMA operation is unaffected by this patch.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Govindraj Raja <govindraj.r@ti.com>
Cc: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Ensure FIFO levels are set correctly in non-DMA mode (the default).
This patch will cause a receive FIFO threshold interrupt to be raised when
there is at least one byte in the RX FIFO. It will also cause a transmit
FIFO threshold interrupt when there is only one byte remaining in the TX
FIFO.
These changes fix the receive interrupt problem and part of the
transmit interrupt problem. A separate set of issues must be worked
around for the transmit path to have a basic level of functionality; a
subsequent patch will address these.
DMA operation is unaffected by this patch.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Govindraj Raja <govindraj.r@ti.com>
Cc: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The function serial_omap_restore_context is called only from
serial_omap_runtime_resume which depends on CONFIG_PM_RUNTIME. Make
serial_omap_restore_context also compile conditionally.
if CONFIG_PM_RUNTIME is not defined below warn may be seen.
LD net/xfrm/built-in.o
drivers/tty/serial/omap-serial.c:1524: warning: 'serial_omap_restore_context' defined but not used
CC drivers/tty/vt/selection.o
Acked-by: Govindraj.R <govindraj.raja@ti.com>
Signed-off-by: Shubhrajyoti D <shubhrajyoti@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The macro SET_SYSTEM_SLEEP_PM_OPS depends CONFIG_PM_SLEEP. The patch
defines the suspend and resume functions for CONFIG_PM_SLEEP instead of
CONFIG_SUSPEND.
Signed-off-by: Shubhrajyoti D <shubhrajyoti@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
There was an error on the jsm driver that would cause it to be unable to
recover after a second error is detected.
At the first error, the device recovers properly:
[72521.485691] EEH: Detected PCI bus error on device 0003:02:00.0
[72521.485695] EEH: This PCI device has failed 1 times in the last hour:
...
[72532.035693] ttyn3 at MMIO 0x0 (irq = 49) is a jsm
[72532.105689] jsm: Port 3 added
However, at the second error, it cascades until EEH disables the device:
[72631.229549] Call Trace:
...
[72641.725687] jsm: Port 3 added
[72641.725695] EEH: Detected PCI bus error on device 0003:02:00.0
[72641.725698] EEH: This PCI device has failed 3 times in the last hour:
It was caused because the PCI state was not being saved after the first
restore. Therefore, at the second recovery the PCI state would not be
restored.
Signed-off-by: Lucas Kannebley Tavares <lucaskt@linux.vnet.ibm.com>
Signed-off-by: Breno Leitao <brenohl@br.ibm.com>
Acked-by: Thadeu Lima de Souza Cascardo <cascardo@linux.vnet.ibm.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The drivers/tty/serial dir is already getting rather busy.
Relocate the 8250 related drivers to their own subdir to
reduce the clutter.
Note that sunsu.c is not included in this move -- it is
8250-like hardware, but it does not use any of the existing
infrastructure -- and does not depend on SERIAL_8250.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
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Merge tag 'rmobile-for-linus' of git://github.com/pmundt/linux-sh
SH/R-Mobile updates for 3.3 merge window.
* tag 'rmobile-for-linus' of git://github.com/pmundt/linux-sh: (32 commits)
arm: mach-shmobile: add a resource name for shdma
ARM: mach-shmobile: r8a7779 SMP support V3
ARM: mach-shmobile: Add kota2 defconfig.
ARM: mach-shmobile: Add marzen defconfig.
ARM: mach-shmobile: r8a7779 power domain support V2
ARM: mach-shmobile: Fix up marzen build for recent GIC changes.
ARM: mach-shmobile: r8a7779 PFC function support
ARM: mach-shmobile: Flush caches in platform_cpu_die()
ARM: mach-shmobile: Allow SoC specific CPU kill code
ARM: mach-shmobile: Fix headsmp.S code to use CPUINIT
ARM: mach-shmobile: clock-r8a7779: clkz/clkzs support
ARM: mach-shmobile: clock-r8a7779: add DIV4 clock support
ARM: mach-shmobile: Marzen LAN89218 support
ARM: mach-shmobile: Marzen SCIF2/SCIF4 support
ARM: mach-shmobile: r8a7779 PFC GPIO-only support V2
ARM: mach-shmobile: r8a7779 and Marzen base support V2
sh: pfc: Unlock register support
sh: pfc: Variable bitfield width config register support
sh: pfc: Add config_reg_helper() function
sh: pfc: Convert index to field and value pair
...
Another simple series related to clock management, this time only for
imx.
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Merge tag 'clk' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc
clock management changes for i.MX
Another simple series related to clock management, this time only for
imx.
* tag 'clk' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc:
ARM: mxs: select HAVE_CLK_PREPARE for clock
clk: add config option HAVE_CLK_PREPARE into Kconfig
ASoC: mxs-saif: convert to clk_prepare/clk_unprepare
video: mxsfb: convert to clk_prepare/clk_unprepare
serial: mxs-auart: convert to clk_prepare/clk_unprepare
net: flexcan: convert to clk_prepare/clk_unprepare
mtd: gpmi-lib: convert to clk_prepare/clk_unprepare
mmc: mxs-mmc: convert to clk_prepare/clk_unprepare
dma: mxs-dma: convert to clk_prepare/clk_unprepare
net: fec: add clk_prepare/clk_unprepare
ARM: mxs: convert platform code to clk_prepare/clk_unprepare
clk: add helper functions clk_prepare_enable and clk_disable_unprepare
Fix up trivial conflicts in drivers/net/ethernet/freescale/fec.c due to
commit 0ebafefcaa ("net: fec: add clk_prepare/clk_unprepare") clashing
trivially with commit e163cc97f9 ("net/fec: fix the .remove code").
A significant part of the changes for these two platforms went into
power management, so they are split out into a separate branch.
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Merge tag 'pm' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc
power management changes for omap and imx
A significant part of the changes for these two platforms went into
power management, so they are split out into a separate branch.
* tag 'pm' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: (65 commits)
ARM: imx6: remove __CPUINIT annotation from v7_invalidate_l1
ARM: imx6: fix v7_invalidate_l1 by adding I-Cache invalidation
ARM: imx6q: resume PL310 only when CACHE_L2X0 defined
ARM: imx6q: build pm code only when CONFIG_PM selected
ARM: mx5: use generic irq chip pm interface for pm functions on
ARM: omap: pass minimal SoC/board data for UART from dt
arm/dts: Add minimal device tree support for omap2420 and omap2430
omap-serial: Add minimal device tree support
omap-serial: Use default clock speed (48Mhz) if not specified
omap-serial: Get rid of all pdev->id usage
ARM: OMAP2+: hwmod: Add a new flag to handle hwmods left enabled at init
ARM: OMAP4: PRM: use PRCM interrupt handler
ARM: OMAP3: pm: use prcm chain handler
ARM: OMAP: hwmod: add support for selecting mpu_irq for each wakeup pad
ARM: OMAP2+: mux: add support for PAD wakeup interrupts
ARM: OMAP: PRCM: add suspend prepare / finish support
ARM: OMAP: PRCM: add support for chain interrupt handler
ARM: OMAP3/4: PRM: add functions to read pending IRQs, PRM barrier
ARM: OMAP2+: hwmod: Add API to enable IO ring wakeup
ARM: OMAP2+: mux: add wakeup-capable hwmod mux entries to dynamic list
...
Both platforms had some initial device tree support, but this adds
much more to actually make it usable.
This is where the really nasty conflicts in the samsung platform
start, due to some files getting moved around and combined in the
'restart' branch that has already gone into mainline through
Russell's tree.
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Merge tag 'dt' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc
Device tree conversions for samsung and tegra
Both platforms had some initial device tree support, but this adds
much more to actually make it usable.
* tag 'dt' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: (45 commits)
ARM: dts: Add intial dts file for EXYNOS4210 SoC, SMDKV310 and ORIGEN
ARM: EXYNOS: Add Exynos4 device tree enabled board file
rtc: rtc-s3c: Add device tree support
input: samsung-keypad: Add device tree support
ARM: S5PV210: Modify platform data for pl330 driver
ARM: S5PC100: Modify platform data for pl330 driver
ARM: S5P64x0: Modify platform data for pl330 driver
ARM: EXYNOS: Add a alias for pdma clocks
ARM: EXYNOS: Limit usage of pl330 device instance to non-dt build
ARM: SAMSUNG: Add device tree support for pl330 dma engine wrappers
DMA: PL330: Add device tree support
ARM: EXYNOS: Modify platform data for pl330 driver
DMA: PL330: Infer transfer direction from transfer request instead of platform data
DMA: PL330: move filter function into driver
serial: samsung: Fix build for non-Exynos4210 devices
serial: samsung: add device tree support
serial: samsung: merge probe() function from all SoC specific extensions
serial: samsung: merge all SoC specific port reset functions
ARM: SAMSUNG: register uart clocks to clock lookup list
serial: samsung: remove all uses of get_clksrc and set_clksrc
...
Fix up fairly trivial conflicts in arch/arm/mach-s3c2440/clock.c and
drivers/tty/serial/Kconfig both due to just adding code close to
changes.
* 'tty-next' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (65 commits)
tty: serial: imx: move del_timer_sync() to avoid potential deadlock
imx: add polled io uart methods
imx: Add save/restore functions for UART control regs
serial/imx: let probing fail for the dt case without a valid alias
serial/imx: propagate error from of_alias_get_id instead of using -ENODEV
tty: serial: imx: Allow UART to be a source for wakeup
serial: driver for m32 arch should not have DEC alpha errata
serial/documentation: fix documented name of DCD cpp symbol
atmel_serial: fix spinlock lockup in RS485 code
tty: Fix memory leak in virtual console when enable unicode translation
serial: use DIV_ROUND_CLOSEST instead of open coding it
serial: add support for 400 and 800 v3 series Titan cards
serial: bfin-uart: Remove ASYNC_CTS_FLOW flag for hardware automatic CTS.
serial: bfin-uart: Enable hardware automatic CTS only when CTS pin is available.
serial: make FSL errata depend on 8250_CONSOLE, not just 8250
serial: add irq handler for Freescale 16550 errata.
serial: manually inline serial8250_handle_port
serial: make 8250 timeout use the specified IRQ handler
serial: export the key functions for an 8250 IRQ handler
serial: clean up parameter passing for 8250 Rx IRQ handling
...
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/jikos/trivial: (53 commits)
Kconfig: acpi: Fix typo in comment.
misc latin1 to utf8 conversions
devres: Fix a typo in devm_kfree comment
btrfs: free-space-cache.c: remove extra semicolon.
fat: Spelling s/obsolate/obsolete/g
SCSI, pmcraid: Fix spelling error in a pmcraid_err() call
tools/power turbostat: update fields in manpage
mac80211: drop spelling fix
types.h: fix comment spelling for 'architectures'
typo fixes: aera -> area, exntension -> extension
devices.txt: Fix typo of 'VMware'.
sis900: Fix enum typo 'sis900_rx_bufer_status'
decompress_bunzip2: remove invalid vi modeline
treewide: Fix comment and string typo 'bufer'
hyper-v: Update MAINTAINERS
treewide: Fix typos in various parts of the kernel, and fix some comments.
clockevents: drop unknown Kconfig symbol GENERIC_CLOCKEVENTS_MIGR
gpio: Kconfig: drop unknown symbol 'CS5535_GPIO'
leds: Kconfig: Fix typo 'D2NET_V2'
sound: Kconfig: drop unknown symbol ARCH_CLPS7500
...
Fix up trivial conflicts in arch/powerpc/platforms/40x/Kconfig (some new
kconfig additions, close to removed commented-out old ones)
* 'amba-modalias' of git://ftp.arm.linux.org.uk/pub/linux/arm/kernel/git-cur/linux-2.6-arm:
sound: aaci: Enable module alias autogeneration for AMBA drivers
watchdog: sp805: Enable module alias autogeneration for AMBA drivers
fbdev: amba: Enable module alias autogeneration for AMBA drivers
serial: pl011: Enable module alias autogeneration for AMBA drivers
serial: pl010: Enable module alias autogeneration for AMBA drivers
spi: pl022: Enable module alias autogeneration for AMBA drivers
rtc: pl031: Enable module alias autogeneration for AMBA drivers
rtc: pl030: Enable module alias autogeneration for AMBA drivers
mmc: mmci: Enable module alias autogeneration for AMBA drivers
input: ambakmi: Enable module alias autogeneration for AMBA drivers
gpio: pl061: Enable module alias autogeneration for AMBA drivers
dmaengine: pl330: Enable module alias autogeneration for AMBA drivers
dmaengine: pl08x: Enable module alias autogeneration for AMBA drivers
hwrng: nomadik: Enable module alias autogeneration for AMBA drivers
ARM: amba: Auto-generate AMBA driver module aliases during modpost
ARM: amba: Move definition of struct amba_id to mod_devicetable.h
del_timer_sync() acquires its own lock and doesn't have to be nested
within the spinlock of sport->port.lock in imx_set_termios(), which
will cause potential deadlock. Fix this by moving it outside.
Cc: Fabio Estevam <fabio.estevam@freescale.com>
Cc: Shawn Guo <shawn.guo@linaro.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Eric Miao <eric.miao@linaro.org>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
These methods are invoked if the iMX uart is used in conjuction with kgdb during
early boot. In order to access the UART without the interrupts, the kernel uses
the basic polling methods for IO with the device. With these methods
implemented, it is now possible to enable kgdb during early boot over serial.
Signed-off-by: Saleem Abdulrasool <compnerd@compnerd.org>
Signed-off-by: Dirk Behme <dirk.behme@gmail.com>
CC: Sascha Hauer <s.hauer@pengutronix.de>
CC: Fabio Estevam <festevam@gmail.com>
CC: Uwe Kleine-Koenig <u.kleine-koenig@pengutronix.de>
CC: linux-serial@vger.kernel.org
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Factor out the uart save/restore functionality instead of
having the same code several times in the driver.
Signed-off-by: Dirk Behme <dirk.behme@gmail.com>
CC: Saleem Abdulrasool <compnerd@compnerd.org>
CC: Sascha Hauer <s.hauer@pengutronix.de>
CC: Fabio Estevam <festevam@gmail.com>
CC: Uwe Kleine-Koenig <u.kleine-koenig@pengutronix.de>
CC: linux-serial@vger.kernel.org
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
When the uart device is instantiated by dt but dt doesn't provide an
alias then better let probing fail instead of falling back to an
unrelated device id used for the line number and no platform data.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
A quick look at of_alias_get_id shows that in the error case it returns
-ENODEV, too, but still it's better style to propagate the value as is.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Cc: Shawn Guo <shawn.guo@linaro.org>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Grant Likely <grant.likely@secretlab.ca>
Cc: Jeremy Kerr <jeremy.kerr@canonical.com>
Cc: Jason Liu <jason.hui@linaro.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Acked-by: Jason Liu <jason.hui@linaro.org>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Allow UART to be a source for wakeup from low power mode.
Tested on a MX27PDK by doing:
echo enabled > /sys/devices/platform/imx21-uart.0/tty/ttymxc0/power/wakeup
echo mem > /sys/power/state
and then pressing a key in the console will wakeup the sytem.
Suggested-by: Shawn Guo <shawn.guo@freescale.com>
Signed-off-by: Fabio Estevam <fabio.estevam@freescale.com>
Tested-by: Richard Zhao <richard.zhao@freescale.com>
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This driver was copied from the original 8250 driver and hence
got the DEC alpha errata workaround. But the workaround is ugly
and we don't really want it in any more places than it absolutely
needs to be. Obviously ARCH=m32r means ARCH != alpha, so just
remove the references to the ALPHA_KLUDGE_MCR define.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Patch to fix a spinlock lockup in the driver that sometimes happens when the
tasklet starts.
Signed-off-by: Claudio Scordino <claudio@evidence.eu.com>
Signed-off-by: Dave Bender <codehero@gmail.com>
Tested-by: Dave Bender <codehero@gmail.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
add support for 400Hv3, 410Hv3 and 800Hv3
Signed-off-by: Yegor Yefremov <yegorslists@googlemail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The patch converts mxs-auart driver to clk_prepare/clk_unprepare by
using helper functions clk_prepare_enable/clk_disable_unprepare.
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Alan Cox <alan@linux.intel.com>
Fix following warnings:
WARNING: drivers/tty/serial/built-in.o(.text+0x7370): Section mismatch in reference from the function grlib_apbuart_configure() to the variable .init.data:apbuart_match
The function grlib_apbuart_configure() references
the variable __initdata apbuart_match.
This is often because grlib_apbuart_configure lacks a __initdata
annotation or the annotation of apbuart_match is wrong.
+ 3 more warnings like this.
There is no guarantee that grlib_apbuart_of_driver.of_match_table
is only used at __init time - so drop the __initdata annotation.
grlib_apbuart_configure() is only used during __init so add __init
to this method too.
Signed-off-by: Sam Ravnborg <sam@ravnborg.org>
Cc: Daniel Hellstrom <daniel@gaisler.com>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
exynos4120_serial_drv_data is only defined when building with support
for Exynos4210 so use the already provided define to ensure that we
don't reference it when building for other SoCs.
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
[kgene.kim@samsung.com: Fixed build warning]
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
Add device tree based discovery support for Samsung's uart controller.
Cc: Ben Dooks <ben-linux@fluff.org>
Acked-by: Grant Likely <grant.likely@secretlab.ca>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
With reset port, set clock and get clock functions in SoC specific extentions
being removed, only the driver probe is left over in these extensions. The
probe function itself can be merged into one and moved into the samsung common
serial driver. With driver probe also moved, all the SoC specific extentions
are no longer required and they are deleted.
Cc: Ben Dooks <ben-linux@fluff.org>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
The port reset function in each of the platform specific extension performs
the same operations and hence all the reset port functions can be merged into
one and moved into the common samsung uart driver. The SoC specific port reset
functions are removed from SoC extensions.
Cc: Ben Dooks <ben-linux@fluff.org>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
With clkdev based clock lookup support, the clock set and get operation
using clock names communicated between the samsung uart driver and the
SoC specific extension can be removed.
In addition to that, for each platform specific extension, add the
default clock selection, number of clock options for uart baud generator,
clock selection bit mask and shift values which is required by the
clkdev support in samsung uart driver.
The default clock selection value 'def_clk_sel' specifies the default clock
to be used as the source clock for baud rate generator in case the platform
code does not specify the same.
Cc: Ben Dooks <ben-linux@fluff.org>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
With clkdev based clock lookup added to samsung serial driver, the use
of 'struct s3c24xx_uart_clksrc' to supply clock names in platform
data is removed from all the Samsung platform code.
Cc: Ben Dooks <ben-linux@fluff.org>
Cc: Ramax Lo <ramaxlo@gmail.com>
Cc: Vasily Khoruzhick <anarsoul@gmail.com>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
Instead of using clock names supplied in platform data, use a generic
clock name 'clk_uart_baud' to look up clocks. The platform code should
register clocks with the name 'clk_uart_baud' which can be used by the
baud rate generator. The clock lookup and selection of the best clock
as baud rate clock is reworked.
Platform code can specify the clocks that can be used as source for the
baud clock (as supported previously by passing names of clocks). A new
member is added to the platform data 'clk_sel' which holds a bit-field
value with each bit representing a baud source clock. If a bit at any
bit position is set, that clock is looked up to participate in the
selection of the baud clock source.
Cc: Ben Dooks <ben-linux@fluff.org>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
s3c2440 uses fclk/n (fclk divided by n) clock as one of the possible clocks used
to generate the baud rate clock. The divider 'n' in this case can be logically
represented outside of the uart controller.
This patch creates a new clock by name "fclk_n" for s3c2440 based platforms to
represent the fclk/n clock in the platform code. This clock provides a get_rate
callback that checks the UCON0/1/2 registers to determine the clock rate. The
samsung uart driver would receive the "fclk_n" clock name as one of the possible
baud rate clock options and the driver need not determine clock rate of fclk/n.
Cc: Ben Dooks <ben-linux@fluff.org>
Cc: Vasily Khoruzhick <anarsoul@gmail.com>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
Add a pointer to the location of the platform data in the driver's private
data. When instantiated using device tree, pdev->dev->platform_data does not
necessarily point to a valid instance of platform data. The platform data
pointer in the driver's private data could be set to pdev->dev->platform_data
or platform data instance created from device tree.
Cc: Ben Dooks <ben-linux@fluff.org>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
Adapt the driver to device tree and pass minimal platform
data from device tree needed for console boot.
No power management features will be suppported for now
since it requires more tweaks around OCP settings
to toggle forceidle/noidle/smartidle bits and handling
remote wakeup and dynamic muxing.
Signed-off-by: Rajendra Nayak <rnayak@ti.com>
Reviewed-by: Rob Herring <rob.herring@calxeda.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Use a default clock speed of 48Mhz, instead of ending up with 0,
if platforms fail to specify a valid clock speed.
Signed-off-by: Rajendra Nayak <rnayak@ti.com>
Reviewed-by: Rob Herring <rob.herring@calxeda.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
With Device tree, pdev->id would no longer be Valid.
Hence get rid of all instances of its usage in the
driver. Device tree support for the driver is added
in subsequent patches.
Signed-off-by: Rajendra Nayak <rnayak@ti.com>
Reviewed-by: Rob Herring <rob.herring@calxeda.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
This patch reworks & simplifies pmac_zilog handling of suspend/resume,
essentially removing all the specific code in there and using the
generic uart helpers.
This required properly registering the tty as a child of the macio (or platform)
device, so I had to delay the registration a bit (we used to register the ports
very very early). We still register the kernel console early though.
I removed a couple of unused or useless flags as well, relying on the
core to not call us when asleep. I also removed the essentially useless
interrupt mutex, simplifying the locking a bit.
I removed some code for handling unexpected interrupt which should never
be hit and could potentially be harmful (causing us to access a register
on a powered off SCC). We diable port interrupts on close always so there
should be no need to drain data on a closed port.
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Fixes below compilation warning.
drivers/tty/serial/omap-serial.c: In function 'serial_omap_irq':
drivers/tty/serial/omap-serial.c:228:29: warning: 'ch' may be used uninitialized in this function [-Wuninitialized]
Fix below sparse warning.
drivers/tty/serial/omap-serial.c:392:52: warning: incorrect type in argument 2 (different signedness)
drivers/tty/serial/omap-serial.c:392:52: expected int *status
drivers/tty/serial/omap-serial.c:392:52: got unsigned int *<noident>
Reported-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Omap_uart_can_sleep function blocks system wide low power state until
uart is active remove this func and add qos requests to prevent
MPU from transitioning.
Keep qos request to default value which will allow MPU to transition
and while uart baud rate is available calculate the latency value
from the baudrate and use the same to hold constraint while uart clocks
are enabled, and if uart is auto-idled the constraint is updated with
default constraint value allowing MPU to transition.
Qos requests are blocking notifier calls so put these requests to
work queue, also the driver uses irq_safe version of runtime API's
and callbacks can be called in interrupt disabled context.
So to avoid warn on slow path warning while using qos update
API's from runtime callbacks use the qos_work_queue.
During bootup the runtime_resume call backs might not be called and runtime
callback gets called only after uart is idled by setting the autosuspend
timeout. So qos_request from runtime resume callback might not activated during
boot if uart baudrate is calculated during bootup for console uart, so schedule
the qos_work queue once we calc_latency while configuring the uart port.
Flush and complete any pending qos jobs in work queue while suspending.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
When using DMA there are two timeouts defined. The first timeout,
rx_timeout, is really a polling rate in which software polls the
DMA status to see if the DMA has finished. This is necessary for
the RX side because we do not know how much data we will receive.
The secound timeout, RX_TIMEOUT, is a timeout after which the
DMA will be stopped if no more data is received. To make this
clearer, rename rx_timeout as rx_poll_rate and rename the
function serial_omap_rx_timeout() to serial_omap_rxdma_poll().
The OMAP-Serial driver defines an RX_TIMEOUT of 3 seconds that is
used to indicate when the DMA for UART can be stopped if no more
data is received. The value is a global definition that is applied
to all instances of the UART.
Each UART may be used for a different purpose and so the timeout
required may differ. Make this value configurable for each UART so
that this value can be optimised for power savings.
Signed-off-by: Jon Hunter <jon-hunter@ti.com>
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
The following UART parameters are defined within the UART driver:
1). Whether the UART uses DMA (dma_enabled), by default set to 0
2). The size of dma buffer (set to 4096 bytes)
3). The time after which the dma should stop if no more data is received.
4). The auto suspend delay that will be passed for pm_runtime_autosuspend
where uart will be disabled after timeout
Different UARTs may be used for different purpose such as the console,
for interfacing bluetooth chip, for interfacing to a modem chip, etc.
Therefore, it is necessary to be able to customize the above settings
for a given board on a per UART basis.
This change allows these parameters to be configured from the board file
and allows the parameters to be configured for each UART independently.
If a board does not define its own custom parameters for the UARTs, then
use the default parameters in the structure "omap_serial_default_info".
The default parameters are defined to be the same as the current settings
in the UART driver to avoid breaking the UART for any cuurnelty supported
boards. By default, make all boards use the default UART parameters.
Signed-off-by: Deepak K <deepak.k@ti.com>
Signed-off-by: Jon Hunter <jon-hunter@ti.com>
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
From the runtime callbacks enable hwmod wakeups for uart which will
internally enable io-pad wakeups for uarts if they have rx-pad pins
set as wakeup capabale.
Use the io-ring wakeup mechanism after uart clock gating and leave
the PM_WKST set for uart to default reset values cleanup the
code in serial.c which was handling PM_WKST reg.
Irq_chaing(PRM_DRIVER) is used to wakeup uart after uart clocks are gated
using pad wakeup mechanism.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Move the errata handling mechanism from serial.c to omap-serial file
and utilise the same func in driver file.
Errata i202, i291 are moved to be handled with omap-serial
Moving the errata macro from serial.c file to driver header file
as from on errata will be handled in driver file itself.
Corrected errata id from chapter reference 2.15 to errata id i291.
Removed errata and dma_enabled fields from omap_uart_state struct
as they are no more needed with errata handling done within omap-serial.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Kevin Hilman <khilman@ti.com>
Avoid unconditional context restore every time we gate uart
clocks. Check whether context loss happened based on which
we can context restore uart regs from uart_port structure.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Remove the uart reset function which is configuring the
TX empty irq which can now be handled within omap-serial driver.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Add missing uart regs to uart_port structure which can be used in
context restore. Store dll, dlh, mdr1, scr, efr, lcr, mcr reg values
into uart_port structure while configuring individual port in termios
function.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Remove context save function from serial.c and move context restore
function to omap-serial. Remove all regs stored in omap_uart_state
for contex_save/restore, reg read write funcs used in context_save/restore,
io_addresses populated for read/write funcs.
Clock gating mechanism was done in serial.c and had no info on uart state
thus we needed context save and restore in serial.c
With runtime conversion and clock gating done within uart driver
context restore can be done from regs value available from uart_omap_port
structure.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Adapts omap-serial driver to use pm_runtime API's.
Use runtime runtime API's to handle uart clocks and obtain
device_usage statics. Set runtime API's usage to irq_safe so that
we can use get_sync from irq context. Auto-suspend for port specific
activities and put for reg access. Moving suspend/resume hooks
to dev_pm_ops structure and bind with config_suspend to avoid any
compilation warning if config_suspend is disabled.
By default uart autosuspend delay is set to -1 to avoid character loss
if uart's are autoidled and woken up on rx pin.
After boot up UART's can be autoidled by setting autosuspend delay from sysfs.
echo 3000 > /sys/devices/platform/omap/omap_uart.X/power/autosuspend_delay_ms
X=0,1,2,3 for UART1/2/3/4. Number of uarts available may vary across omap_soc.
Also if uart is not wakeup capable we can prevent runtime autosuspend by
forbiding runtime.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Kevin Hilman <khilman@ti.com>
The mapbase (start_address), membase(io_remap cookie) part of
pdata struct omap_uart_port_info are removed as this should be
derived within driver.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Currently we use a shared irq handler to identify uart activity and then
trigger a timer. By default the timeout value is zero and can be set or
modified from sysfs. If there was no uart activity for the period set
through sysfs, the timer will expire and call timer handler this will
set a flag can_sleep using which decision to gate uart clocks can be taken.
Since the clock gating mechanism is outside the uart driver, we currently
use this mechanism. In preparation to runtime implementation for omap-serial
driver we can cleanup this mechanism and use runtime API's to gate uart clocks.
Removes the following:
* timer related info from local uart_state struct
* the code used to set timeout value from sysfs.
* irqflags used to set shared irq handler.
* un-used function omap_uart_check_wakeup.
Signed-off-by: Govindraj.R <govindraj.raja@ti.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes)
Signed-off-by: Kevin Hilman <khilman@ti.com>
Blackfin uart supports automatic CTS trigger when hardware flow control is enabled.
No need to start and top tx in CTS interrupt. So, remote ASYNC_CTS_FLOW flag.
Signed-off-by: Sonic Zhang <sonic.zhang@analog.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The recent commit "serial: add irq handler for Freescale 16550 errata"
would allow Kconfig choices that had 8250 support as a module and
yet still try and build in the errata fix non-modular, resulting
in build failures for some non-embedded PPC targets.
Since we hook in the errata fix from legacy_serial.c, which is
built only for PPC_UDBG_16550, and since the errata is only really
relevant for SysRQ on serial console, tighten up the dependencies
to be exactly that.
We'll get coverage on the relevant Freescale boards because the
Kconfig for their CPU types all select the PPC_UDBG_16550 option,
and the defconfigs also all select the 8250_CONSOLE option. Also,
the 8250_CONSOLE option has a strict dependency on "SERIAL_8250=y"
which resolves the reported problem for non Freescale targets.
Reported-by: Michael Neuling <mikey@neuling.org>
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Tested-by: Michael Neuling <mikey@neuling.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Sending a break on the SOC UARTs found in some MPC83xx/85xx/86xx
chips seems to cause a short lived IRQ storm (/proc/interrupts
typically shows somewhere between 300 and 1500 events). Unfortunately
this renders SysRQ over the serial console completely inoperable.
The suggested workaround in the errata is to read the Rx register,
wait one character period, and then read the Rx register again.
We achieve this by tracking the old LSR value, and on the subsequent
interrupt event after a break, we don't read LSR, instead we just
read the RBR again and return immediately.
The "fsl,ns16550" is used in the compatible field of the serial
device to mark UARTs known to have this issue.
Thanks to Scott Wood for providing the errata data which led to
a much cleaner fix.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Currently serial8250_handle_irq is a trivial wrapper around
serial8250_handle_port, which actually does all the work.
Since there are no other callers of serial8250_handle_port, we
can just move it inline into serial8250_handle_irq. This also
makes it more clear what functionality any custom IRQ handlers
need to provide if not using serial8250_default_handle_irq.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The current 8250 timeout code duplicates the code path in
serial8250_default_handle_irq and then serial8250_handle_irq
i.e. reading iir, check for IIR_NO_INT, and then calling
serial8250_handle_port.
So the immediate thought is to replace the duplicated code
with a call to serial8250_default_handle_irq.
But this highlights a problem. We let 8250 driver variants
use their own IRQ handler via specifying their own custom
->handle_irq, but in the event of a timeout, we ignore their
handler and implicitly run serial8250_default_handle_irq instead.
So, go through the struct to get ->handle_irq and call that,
which for most will still be serial8250_default_handle_irq.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
For drivers that need to construct their own IRQ handler, the
three components are seen in the current handle_port -- i.e.
Rx, Tx and modem_status.
Make these exported symbols so that "almost" 8250 UARTs can
construct their own IRQ handler with these shared components,
while working around their own unique errata issues.
The function names are given a serial8250 prefix, since they
are now entering the global namespace.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The receive_chars() was taking a pointer to a passed in LSR value
in status and knocking off bits as it processed them. But since
receive_chars isn't returning a value, we can instead pass in
a normal non-pointer value for LSR, and simply return the
residual (unprocessed) LSR once it is done.
The value in this cleanup, is that it clarifies the API of the
receive_chars prior to exporting it to other 8250-like drivers
for shared usage.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Since we want to promote sharing and move away from one single
uart driver with a bunch of platform specific bugfixes all
munged into one, relocate some header like material from
the C file to the header.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
msm_hs_handle_delta_cts tries to acquire port->lock already acquired
by the callee function msm_hs_isr. Change function name to follow
"_locked" convention.
Signed-off-by: Mayank Rana <mrana@codeaurora.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Both tx and rx command_ptr_ptr are of type u32*. While allocating
memory for it, sizeof(u32 *) is used as part of kmalloc API instead
of sizeof(u32). ADM Hardare requires size of command_ptr_ptr as 1 Word.
Both sizeof(u32 *) and sizeof(u32) are same on 32-bit architecture
whereas sizeof(u32 *) would be different in size compare to sizeof(u32)
on anyother architecture.
Hence correct usage of sizeof(command_ptr_ptr) for Tx and Rx with
kmalloc and dma_(map/unmap)_single APIs.
Signed-off-by: Mayank Rana <mrana@codeaurora.org>
Reported-by: Ilia Mirkin <imirkin@alum.mit.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Current serial_cs driver has a problem when trying to detect whether
a card has multiple ports: serial_config() calls pcmcia_loop_config()
which iterates over card CIS configurations by calling
serial_check_for_multi() for each of them.
This function wants to check (and select) a configuration
that has either one long I/O window spanning multiple ports or two 8-port
windows for two serial ports.
Problem is, that every pcmcia_loop_config() iteration only updates
the windows (via pcmcia_do_loop_config() in resource[0] and resource[1])
when CONF_AUTO_SET_IO flag is set on the device, which is set only later
in the code.
Fix it by setting this flag earlier.
In addition to this, when multi-port card is detected
and it does not have an one, long I/O window
multi_config_check_notpicky() tries to locate two I/O windows and assumes
they are continuous without checking.
On an Argosy RS-COM 2P this selects first configuration, which
unfortunately has two non-continuous I/O windows.
The net effect is that the second serial port on the card does not work.
Fix it by checking whether the windows are really continuous.
Signed-off-by: Maciej Szmigiero <mhej@o2.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Makes it easier to find all occurences requesting CONF_MODE_B.
Signed-off-by: Wolfram Sang <w.sang@pengutronix.de>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This patch is similar to that for bfin-uart hardware flow control.
Sport emulated serial device may be probed earlier before GPIOLIB is initialized.
Requesting and configuring CTS GPIO PIN fails in that early stage.
Signed-off-by: Sonic Zhang <sonic.zhang@analog.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Blackfin hardware CTS control generate interrupt for both CTS on and off.
Signed-off-by: Sonic Zhang <sonic.zhang@analog.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Serial device may be probed earlier before GPIOLIB is initialized. Requesting and
configuring CTS GPIO PIN fails in that early stage. Do it when the serial device
really starts up.
Signed-off-by: Sonic Zhang <sonic.zhang@analog.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
On most 68k Macs the SCC IRQ is an autovector interrupt and cannot be
masked. This can be a problem when pmac_zilog starts up.
For example, the serial debugging code in arch/m68k/kernel/head.S may be
used beforehand. It disables the SCC interrupts at the chip but doesn't
ack them. Then when a pmac_zilog port is used, the machine locks up with
"unexpected interrupt".
This can happen in pmz_shutdown() since the irq is freed before the
channel interrupts are disabled.
Fix this by clearing interrupt enable bits before the handler is
uninstalled. Also move the interrupt control bit flipping into a separate
pmz_interrupt_control() routine. Replace all instances of these operations
with calls to this routine. Omit the zssync() calls that seem to serve no
purpose.
Signed-off-by: Finn Thain <fthain@telegraphics.com.au>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
This patch adds the driver for the built-in UART of the
Atheros AR933X SoCs.
Signed-off-by: Gabor Juhos <juhosg@openwrt.org>
Cc: linux-mips@linux-mips.org
Cc: Kathy Giori <kgiori@qca.qualcomm.com>
Cc: "Luis R. Rodriguez" <rodrigue@qca.qualcomm.com>
Cc: Alan Cox <alan@lxorguk.ukuu.org.uk>
Cc: linux-serial@vger.kernel.org
Patchwork: https://patchwork.linux-mips.org/patch/2526/
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Ralf Baechle <ralf@linux-mips.org>
This adds initial support for requesting the various GPIO functions
necessary for certain ports. This just plugs in dumb request/free logic,
but serves as a building block for migrating off of the ->init_pins mess
to a wholly gpiolib backed solution (primarily parts with external
RTS/CTS pins, but will also allow us to clean up RXD pin testing).
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
When toggling the MCE support we don't want to concern ourselves with the
FIFO state, so ensure that the clearing bits are masked out when updating
the MCE state.
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
The bulk of the ports do not support any sort of modem control, so
blindly twiddling the MCE bit doesn't accomplish much. We now require
ports to manually specify which line supports modem control signals.
While at it, tidy up the RTS/CTSIO handling in SCSPTR parts so it's a bit
more obvious what's going on (and without clobbering other configurations
in the process).
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
This patch converts the drivers in drivers/tty/serial/* to use the
module_platform_driver() macro which makes the code smaller and a bit
simpler.
Cc: Arnd Bergmann <arnd@arndb.de>
Cc: Jamie Iles <jamie@jamieiles.com>
Cc: Yoichi Yuasa <yuasa@linux-mips.org>
Signed-off-by: Axel Lin <axel.lin@gmail.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
In ancient times it was necessary to manually initialize the bus field of an
spi_driver to spi_bus_type. These days this is done in spi_driver_register(),
so we can drop the manual assignment.
The patch was generated using the following coccinelle semantic patch:
// <smpl>
@@
identifier _driver;
@@
struct spi_driver _driver = {
.driver = {
- .bus = &spi_bus_type,
},
};
// </smpl>
Signed-off-by: Lars-Peter Clausen <lars@metafoo.de>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The semantics of UPF_IIR_ONCE (once per serial irq) are only guaranteed
if the kt irq is not shared (once per serial isr in the shared case ==
potentially unwanted reads of the IIR).
Signed-off-by: Dan Williams <dan.j.williams@intel.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Workaround dropped notifications in the iir register. Prevent reads
coincident with new interrupt notifications by reading the iir at most
once per interrupt.
Reported-by: Nhan H Mai <nhan.h.mai@intel.com>
Signed-off-by: Dan Williams <dan.j.williams@intel.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
There is no need to call uart_write_wakeup after each character send.
Once at the end of the write sequence is enough.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The function check_modem_status returns an int currently it
is stored in a char.
Signed-off-by: Shubhrajyoti D <shubhrajyoti@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This plugs in loopback control for SCFCR-enabled ports and plugs it in
via the TIOCM_LOOP control, as others do.
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
At the moment things like CTS/RTS are reported for all ports, while the
vast majority of them do not implement support at all (and others
implement support entirely in hardware). Fix up the ->get_mctrl()
reporting to simply assert DSR/CAR as other drivers without control
lines do.
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
Technically there's nothing we can do for either of these, so update the
comments to reflect this, rather than infering that there's additional
work to be done.
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
Presently the icount stats are only adjusted for the rx/tx case, this
makes sure that they're updated appropriately for the non-tx/rx cases,
too (specifically overruns, breaks, as well as frame and parity errors).
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
Presently there are a few places that make assumptions about the
existence of SCFCR, which doesn't hold true for several port types. While
generally harmless, this does lead to bogus reads/writes in both the
termios/runtime PM cases that are better off simply never being made in
the first place.
While we're at it, also get rid of a straggling PORT_SCI check that
infers all non-SCI ports contain SCFCR. This doesn't presently have any
impact, but as we're now able to test for the existence of registers
without defering to the port type we future proof for additional port
types.
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
The UCC UART driver is missing a call to uart_update_timeout().
Without this call, attempting to close the port after outputting large
amounts of data (i.e. using tty and uart buffering) results in long
timeouts before the port will actually be shut down.
For example, cat a large file to a UCC UART port. With the current
driver, the port will stay open for 30 seconds after the last byte
of data is output. But with this patch, the port is closed as
expected, just after the data has been output (tx fifos empty).
Signed-off-by: Chuck Meade <chuck@ThePTRGroup.com>
Acked-by: Timur Tabi <timur@freescale.com>
Signed-off-by: Kumar Gala <galak@kernel.crashing.org>
Commit 8c8fdbc9bd ("[ARM] Remove arch-imx from build system") dropped
ARCH_IMX. So this last reference to ARCH_IMX has been an
(inconsequential) nop since v2.6.31. And because ARCH_MXC practically
implies ARM we can also drop the reference to the latter symbol.
Signed-off-by: Paul Bolle <pebolle@tiscali.nl>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
* 'tty-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty:
TTY: ldisc, wait for ldisc infinitely in hangup
TTY: ldisc, move wait idle to caller
TTY: ldisc, allow waiting for ldisc arbitrarily long
Revert "tty/serial: Prevent drop of DCD on suspend for Tegra UARTs"
RS485: fix inconsistencies in the meaning of some variables
pch_uart: Fix DMA resource leak issue
serial,mfd: Fix CMSPAR setup
tty/serial: Prevent drop of DCD on suspend for Tegra UARTs
pch_uart: Change company name OKI SEMICONDUCTOR to LAPIS Semiconductor
pch_uart: Support new device LAPIS Semiconductor ML7831 IOH
pch_uart: Fix hw-flow control issue
tty: hvc_dcc: Fix duplicate character inputs
jsm: Change maintainership
SiRFprimaII is the latest generation application processor from CSR’s
multi-function SoC product family.
The SoC support codes are in arch/arm/mach-prima2 from Linux mainline
3.0.
There are three dedicated UARTs in system. This patch adds basic driver
support for them.
It has used the newest pinmux subsystem from Linus Walleij.
Cc: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Rong Wang <Rong.Wang@csr.com>
Signed-off-by: Bin Shi <Bin.Shi@csr.com>
Signed-off-by: Barry Song <Baohua.Song@csr.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This reverts commit 9636b755da.
It wasn't supposed to be applied, thanks to Doug for letting me know.
Cc: Doug Anderson <dianders@chromium.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Extract ASYNC_INITIALIZED/TTY_IO_ERROR handling from uart_startup.
This will be useful for tty port helpers. These flags are handled
by the helpers instead.
So we create a new function uart_port_startup without touching these
flags there. And we keep uart_startup with the exact behavior as
before. We need that one because we start/stop the device from other
paths than open/close/hangup.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Let's fill the port_ops->shutdown. We will need this for hangup and
close port helpers.
We don't need to touch DTR/RTS registers in uart_port_shutdown. They
are set to off from port_close_start properly already.
Also we don't need to pin the TTY_IO_ERROR bit. This will be done in
close/hangup paths.
We leave uart_shutdown as is, because it is used (and will be) from
several paths now. Like from suspend.
The point is to not touch ASYNC_INITIALIZED bit. It will be set (and
checked) properly by the tty port helpers.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This is a preparation for the next patches which will move the stuff
from uart_open and uart_close/hangup here. Then we will use
tty_port_* helpers.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
We need to expand uart_get into uart_open. We need it to move on with
conversion to use tty_port_open helper. After we do this, the code
will be much more similar to what tty_port_open does.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
It is not used at all, so no need to play any games with that.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Just put a kernel-doc comment to uart_change_pm and uart_insert_char.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
After the previous patches, the code is almost identical. There are
few differences in the helper code:
1) flush_buffer when flow_stopped
* when a user doesn't care about the data, delete it anyways
2) ASYNCB_INITIALIZED test before wait_until_sent_from
* obviously, there is nothing to wait for if the port is dead
3) drain_delay wait
* we don't set drain_delay
So we can use the helper now. It indeed removes a bunch of duplicated
code.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
As the tty_port helpers think closing_wait and close_delay are in
jiffies and we want to use the helpers (next patches), we have to
switch the closing_wait and close_delay from ms to jiffies now.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Current ldisc number is passed as a paramneter -- no need to dig it
out of the tty or ldisc. So switch PPS check to that.
No tty callback can be called with port->line higher than TTY driver
num. So remove the check.
This removes some port.tty users.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Viktar Palstsiuk <viktar.palstsiuk@promwad.com>
Cc: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
There are some functions (uart_handle_dcd_change, _handle_cts_change,
_insert_char) which are big enough to not be inlined. So move them
from .h to .c. We need to export them so that modules can actually use
them.
They will be even bigger when we introduce tty refcounting to them.
While at it, cleanup the "Proud member of Uglyhacks'R'US". It means,
define uart_handle_sysrq_char only when SUPPORT_SYSRQ is set.
Otherwise define it as a macro. This is needed for some arm driver
where the second parameter is undefined if expanded.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Making SERIAL_OMAP depend on ARCH_OMAP2PLUS instead of
oring with ARCH2/3/4.
Acked-by: Felipe Balbi <balbi@ti.com>
Suggested-by: Sricharan R <r.sricharan@ti.com>
Signed-off-by: Shubhrajyoti D <shubhrajyoti@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Add console support to pch_uart. To enable append e.g.
console=ttyPCH0,115200 to your kernel command line.
This is not expected work on CM-iTC boards due to their having a different
clock.
Signed-off-by: Alexander Stein <alexander.stein@systec-electronic.com>
Cc: Alan Cox <alan@lxorguk.ukuu.org.uk>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Add support to specify which HSU port to use as an early console. This can
be selected by passing "earlyprintk=hsu<n>" on the kernel command line. By
default port 0 is still used.
Signed-off-by: Mika Westerberg <mika.westerberg@linux.intel.com>
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
The crisv10.c and the atmel_serial.c serial drivers intepret the fields of the
serial_rs485 structure in a different way.
In particular, crisv10.c uses SER_RS485_RTS_AFTER_SEND and
SER_RS485_RTS_ON_SEND for the voltage of the RTS pin; atmel_serial.c,
instead, uses these values to know if a delay must be set before and
after sending. This patch makes the usage of these variables consistent
across all drivers and fixes the Documentation as well.
From now on, SER_RS485_RTS_AFTER_SEND and SER_RS485_RTS_ON_SEND will be
used to set the voltage of the RTS pin (as in the crisv10.c driver); the
delay will be understood by looking only at the value of
delay_rts_before_send and delay_rts_after_send.
Signed-off-by: Claudio Scordino <claudio@evidence.eu.com>
Signed-off-by: Darron Black <darron@griffin.net>
Acked-by: Jesper Nilsson <jesper.nilsson@axis.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Alan Cox <alan@lxorguk.ukuu.org.uk>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Changing UART mode PIO->DMA->PIO->DMA like below, pch_uart driver can't get
DMA channel resource.
setserial /dev/ttyPCH0 ^low_latency
setserial /dev/ttyPCH0 low_latency
CAUSE:
Changing mode using setserial command, ".startup" function which gets DMA
channel is called before ".verify_port" function which sets
dma-flag(use_dma/use_dma_flag) as 1.
PIO->DMA
.startup: Since dma-flag is 0, DMA channel is not requested.
.verify_port: dma-flag is set as 1.
.shutdown: N/A
DMA->PIO
.startup: Since dma-flag is 1, DMA channel is requested.
.verify_port: dma-flag is set as 0.
.shutdown: Since dma-flag is 0, DMA channel is not released.
This means DMA channel resource leak occurs.
Next time, this driver can't get DMA channel resource forever.
MODIFICATION:
Currently, when release DMA channel resource, this driver checks dma-flag.
However, this specification occurs the above issue.
This driver must check whether dma_request_channel is executed or not.
The values are saved in private data variable "chan_tx/chan_tx".
These variables mean if the value is NULL, DMA channel is not requested,
if not NULL, DMA channel is requested.
This patch fixes the issue.
Signed-off-by: Tomoya MORINAGA <tomoya.rohm@gmail.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This is referenced the wrong way. Mika Westerberg added some checks to the
tty to support multiple console, but the real problem is simply referencing the
termios object via the wrong path.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
On Tegra UARTs (except UART1), the DTR / DCD / DSR lines are not
externally accessible. Instead, the DTR line internally appears to be
looped back to be the input to the DCD and DSR lines. The net effect
of this is that when we drop DTR (like when we suspend), we'll see DCD
drop too. ...and when we see DCD drop, we treat that as a hangup.
In order to prevent this hangup from occurring at every sleep, we need
to force DTR to remain high on Tegra UARTs.
This patch uses the mcr_mask / mcr_force fields, which were originally
added for the kludge ALPHA_KLUDGE_MCR. Using these fields does not
prevent us from removing ALPHA_KLUDGE_MCR--we can just remove the "if"
tests I have added and always init mcr_mask / mcr_force from the
serial8250_config.
NOTE: If we have people that are using UARTA on a Tegra and need to
control DTR, we'll need to either add a separate port type for UARTA
or we'll need to add some tegra-specific code to detect whether the
DTR needs to be left high.
Signed-off-by: Doug Anderson <dianders@chromium.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
On October 1 in 2011,
OKI SEMICONDUCTOR Co., Ltd. changed the company name in to LAPIS Semiconductor Co., Ltd.
Signed-off-by: Tomoya MORINAGA <tomoya-linux@dsn.lapis-semi.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Using hardware flow control,
currently, register of the control-bit(AFE) is not set.
This patch fixes the issue.
Signed-off-by: Tomoya MORINAGA <tomoya-linux@dsn.lapis-semi.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
This adds preliminary support for the R8A7740 (R-Mobile A1) CPU
Timer, serial, gic, clock are supported at this point.
This patch is based on v0.1 manual
Signed-off-by: Kuninori Morimoto <kuninori.morimoto.gx@renesas.com>
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
* 'modsplit-Oct31_2011' of git://git.kernel.org/pub/scm/linux/kernel/git/paulg/linux: (230 commits)
Revert "tracing: Include module.h in define_trace.h"
irq: don't put module.h into irq.h for tracking irqgen modules.
bluetooth: macroize two small inlines to avoid module.h
ip_vs.h: fix implicit use of module_get/module_put from module.h
nf_conntrack.h: fix up fallout from implicit moduleparam.h presence
include: replace linux/module.h with "struct module" wherever possible
include: convert various register fcns to macros to avoid include chaining
crypto.h: remove unused crypto_tfm_alg_modname() inline
uwb.h: fix implicit use of asm/page.h for PAGE_SIZE
pm_runtime.h: explicitly requires notifier.h
linux/dmaengine.h: fix implicit use of bitmap.h and asm/page.h
miscdevice.h: fix up implicit use of lists and types
stop_machine.h: fix implicit use of smp.h for smp_processor_id
of: fix implicit use of errno.h in include/linux/of.h
of_platform.h: delete needless include <linux/module.h>
acpi: remove module.h include from platform/aclinux.h
miscdevice.h: delete unnecessary inclusion of module.h
device_cgroup.h: delete needless include <linux/module.h>
net: sch_generic remove redundant use of <linux/module.h>
net: inet_timewait_sock doesnt need <linux/module.h>
...
Fix up trivial conflicts (other header files, and removal of the ab3550 mfd driver) in
- drivers/media/dvb/frontends/dibx000_common.c
- drivers/media/video/{mt9m111.c,ov6650.c}
- drivers/mfd/ab3550-core.c
- include/linux/dmaengine.h
* 'next' of git://git.kernel.org/pub/scm/linux/kernel/git/benh/powerpc: (106 commits)
powerpc/p3060qds: Add support for P3060QDS board
powerpc/83xx: Add shutdown request support to MCU handling on MPC8349 MITX
powerpc/85xx: Make kexec to interate over online cpus
powerpc/fsl_booke: Fix comment in head_fsl_booke.S
powerpc/85xx: issue 15 EOI after core reset for FSL CoreNet devices
powerpc/8xxx: Fix interrupt handling in MPC8xxx GPIO driver
powerpc/85xx: Add 'fsl,pq3-gpio' compatiable for GPIO driver
powerpc/86xx: Correct Gianfar support for GE boards
powerpc/cpm: Clear muram before it is in use.
drivers/virt: add ioctl for 32-bit compat on 64-bit to fsl-hv-manager
powerpc/fsl_msi: add support for "msi-address-64" property
powerpc/85xx: Setup secondary cores PIR with hard SMP id
powerpc/fsl-booke: Fix settlbcam for 64-bit
powerpc/85xx: Adding DCSR node to dtsi device trees
powerpc/85xx: clean up FPGA device tree nodes for Freecsale QorIQ boards
powerpc/85xx: fix PHYS_64BIT selection for P1022DS
powerpc/fsl-booke: Fix setup_initial_memory_limit to not blindly map
powerpc: respect mem= setting for early memory limit setup
powerpc: Update corenet64_smp_defconfig
powerpc: Update mpc85xx/corenet 32-bit defconfigs
...
Fix up trivial conflicts in:
- arch/powerpc/configs/40x/hcu4_defconfig
removed stale file, edited elsewhere
- arch/powerpc/include/asm/udbg.h, arch/powerpc/kernel/udbg.c:
added opal and gelic drivers vs added ePAPR driver
- drivers/tty/serial/8250.c
moved UPIO_TSI to powerpc vs removed UPIO_DWAPB support
* 'next' of git://git.infradead.org/users/vkoul/slave-dma: (63 commits)
dmaengine: mid_dma: mask_peripheral_interrupt only when dmac is idle
dmaengine/ep93xx_dma: add module.h include
pch_dma: Reduce wasting memory
pch_dma: Fix suspend issue
dma/timberdale: free_irq() on an error path
dma: shdma: transfer based runtime PM
dmaengine: shdma: protect against the IRQ handler
dmaengine i.MX DMA/SDMA: add missing include of linux/module.h
dmaengine: delete redundant chan_id and chancnt initialization in dma drivers
dmaengine/amba-pl08x: Check txd->llis_va before freeing dma_pool
dmaengine/amba-pl08x: Add support for sg len greater than one for slave transfers
serial: sh-sci: don't filter on DMA device, use only channel ID
ARM: SAMSUNG: Remove Samsung specific enum type for dma direction
ASoC: Samsung: Update DMA interface
spi/s3c64xx: Merge dma control code
spi/s3c64xx: Add support DMA engine API
ARM: SAMSUNG: Remove S3C-PL330-DMA driver
ARM: S5P64X0: Use generic DMA PL330 driver
ARM: S5PC100: Use generic DMA PL330 driver
ARM: S5PV210: Use generic DMA PL330 driver
...
Fix up fairly trivial conflicts in
- arch/arm/mach-exynos4/{Kconfig,clock.c}
- arch/arm/mach-s5p64x0/dma.c
This fixes up support for SH-2(A) SCIFs by introducing a new regtype. As
expected, it's close to the SH-4A SCIF with fifodata, but still different
enough to warrant its own type.
Fixes up a number of FIFO overflows and similar for both SH7203/SH7264.
Signed-off-by: Phil Edworthy <phil.edworthy@renesas.com>
Tested-by: Federico Fuga <fuga@studiofuga.com>
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
* 'next/dt' of git://git.linaro.org/people/arnd/arm-soc:
ARM: gic: use module.h instead of export.h
ARM: gic: fix irq_alloc_descs handling for sparse irq
ARM: gic: add OF based initialization
ARM: gic: add irq_domain support
irq: support domains with non-zero hwirq base
of/irq: introduce of_irq_init
ARM: at91: add at91sam9g20 and Calao USB A9G20 DT support
ARM: at91: dt: at91sam9g45 family and board device tree files
arm/mx5: add device tree support for imx51 babbage
arm/mx5: add device tree support for imx53 boards
ARM: msm: Add devicetree support for msm8660-surf
msm_serial: Add devicetree support
msm_serial: Use relative resources for iomem
Fix up conflicts in arch/arm/mach-at91/{at91sam9260.c,at91sam9g45.c}
With module.h being implicitly everywhere via device.h, the absence
of explicitly including something for EXPORT_SYMBOL went unnoticed.
Since we are heading to fix things up and clean module.h from the
device.h file, we need to explicitly include these files now.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
We are cleaning up the issue that means module.h is omnipresent.
These tty users are the people who implictly are relying on that.
Fix up the real users to call out the include that they really need.
In the case of jsm_driver.c file, it had moduleparam.h but that
isn't enough and it needs the full module.h
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
fixup usage of dma direction by introducing dma_transfer_direction,
this patch moves spi, serial drivers to use new enum
Signed-off-by: Vinod Koul <vinod.koul@linux.intel.com>
Cc: Grant Likely <grant.likely@secretlab.ca>
Cc: Alan Cox <alan@linux.intel.com>
Acked-by: Mika Westerberg <mika.westerberg@iki.fi>
* 'spi/next' of git://git.secretlab.ca/git/linux-2.6:
drivercore: Add helper macro for platform_driver boilerplate
spi: irq: Remove IRQF_DISABLED
OMAP: SPI: Fix the trying to free nonexistent resource error
spi/spi-ep93xx: add module.h include
spi/tegra: fix compilation error in spi-tegra.c
spi: spi-dw: fix all sparse warnings
spi/spi-pl022: Call pl022_dma_remove(pl022) only if enable_dma is true
spi/spi-pl022: calculate_effective_freq() must set rate <= requested rate
spi/spi-pl022: Don't allocate more sg than required.
spi/spi-pl022: Use GFP_ATOMIC for allocation from tasklet
spi/spi-pl022: Resolve formatting issues
* 'clk' of http://ftp.arm.linux.org.uk/pub/linux/arm/kernel/git-cur/linux-2.6-arm:
ARM: 7131/1: clkdev: Add Common Macro for clk_lookup
clk: spi-pl022: convert to clk_prepare()/clk_unprepare()
clk: timer-sp: convert to clk_prepare()/clk_unprepare()
clk: sa1111: convert to clk_prepare()/clk_unprepare()
clk: mmci: convert to clk_prepare()/clk_unprepare()
clk: amba-pl011: convert to clk_prepare()/clk_unprepare()
clk: amba-pl010: convert to clk_prepare()/clk_unprepare()
clk: amba-clcd: convert to clk_prepare()/clk_unprepare()
clk: amba bus: convert to clk_prepare()/clk_unprepare()
clk: provide prepare/unprepare functions
* 'tty-next' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (79 commits)
TTY: serial_core: Fix crash if DCD drop during suspend
tty/serial: atmel_serial: bootconsole removed from auto-enumerates
Revert "TTY: call tty_driver_lookup_tty unconditionally"
tty/serial: atmel_serial: add device tree support
tty/serial: atmel_serial: auto-enumerate ports
tty/serial: atmel_serial: whitespace and braces modifications
tty/serial: atmel_serial: change platform_data variable name
tty/serial: RS485 bindings for device tree
TTY: call tty_driver_lookup_tty unconditionally
TTY: pty, release tty in all ptmx_open fail paths
TTY: make tty_add_file non-failing
TTY: drop driver reference in tty_open fail path
8250_pci: Fix kernel panic when pch_uart is disabled
h8300: drivers/serial/Kconfig was moved
parport_pc: release IO region properly if unsupported ITE887x card is found
tty: Support compat_ioctl get/set termios_locked
hvc_console: display printk messages on console.
TTY: snyclinkmp: forever loop in tx_load_dma_buffer()
tty/n_gsm: avoid fifo overflow in gsm_dlci_data_output
tty/n_gsm: fix a bug in gsm_dlci_data_output (adaption = 2 case)
...
Fix up Conflicts in:
- drivers/tty/serial/8250_pci.c
Trivial conflict with removed duplicate device ID
- drivers/tty/serial/atmel_serial.c
Annoying silly conflict between "specify the port num via
platform_data" and other changes to atmel_console_init
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/jikos/trivial: (59 commits)
MAINTAINERS: linux-m32r is moderated for non-subscribers
linux@lists.openrisc.net is moderated for non-subscribers
Drop default from "DM365 codec select" choice
parisc: Kconfig: cleanup Kernel page size default
Kconfig: remove redundant CONFIG_ prefix on two symbols
cris: remove arch/cris/arch-v32/lib/nand_init.S
microblaze: add missing CONFIG_ prefixes
h8300: drop puzzling Kconfig dependencies
MAINTAINERS: microblaze-uclinux@itee.uq.edu.au is moderated for non-subscribers
tty: drop superfluous dependency in Kconfig
ARM: mxc: fix Kconfig typo 'i.MX51'
Fix file references in Kconfig files
aic7xxx: fix Kconfig references to READMEs
Fix file references in drivers/ide/
thinkpad_acpi: Fix printk typo 'bluestooth'
bcmring: drop commented out line in Kconfig
btmrvl_sdio: fix typo 'btmrvl_sdio_sd6888'
doc: raw1394: Trivial typo fix
CIFS: Don't free volume_info->UNC until we are entirely done with it.
treewide: Correct spelling of successfully in comments
...
For simple modules that contain a single platform_driver without any
additional setup code then ends up being a block of duplicated
boilerplate. This patch adds a new macro, module_platform_driver(),
which replaces the module_init()/module_exit() registrations with
template functions.
Signed-off-by: Grant Likely <grant.likely@secretlab.ca>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de>
Reviewed-by: Magnus Damm <magnus.damm@gmail.com>
Reviewed-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Reviewed-by: Stephen Boyd <sboyd@codeaurora.org>
This crash was showing up 100% of the time on Tegra CPUs when an
agetty was running on the serial port and the console was not running
on the serial port. The reason the Tegra saw it so reliably is that
the Tegra CPU internally ties DTR to DCD/DSR. That means when we
dropped DTR during suspend we would get always get an immediate DCD
drop.
The specific order of operations that were running:
* uart_suspend_port() would be called to put the uart in suspend mode
* we'd drop DTR (ops->set_mctrl(uport, 0)).
* the DTR drop would be looped back in the CPU to be a DCD drop.
* the DCD drop would look to the serial driver as a hangup
* the hangup would call uart_shutdown()
* ... suspend / resume happens ...
* uart_resume_port() would be called and run the code in the
(port->flags & ASYNC_SUSPENDED) block, which would startup the port
(and enable tx again).
* Since the UART would be available for tx, we'd immediately get
an interrupt, eventually calling transmit_chars()
* The transmit_chars() function would crash. The first crash would
be a dereference of a NULL tty member, but since the port has been
shutdown that was just a symptom.
I have proposed a patch that would fix the Tegra CPUs here (see
https://lkml.org/lkml/2011/10/11/444 - tty/serial: Prevent drop of DCD
on suspend for Tegra UARTs). However, even with that fix it is still
possible for systems that have an externally visible DCD line to see a
crash if the DCD drops at just the right time during suspend: thus
this patch is still useful.
Signed-off-by: Doug Anderson <dianders@chromium.org>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Auto-enumerate mechanism conflicts with bootconsoles: remove
the usage counter for this type of consoles.
Signed-off-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Will use aliases to enumerate ports, if available.
Signed-off-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Grant Likely <grant.likely@secretlab.ca>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
If no platform data provided to enumerate ports, use a bit field
to choose port number and check if port is already initialized.
Use this mechanism for both console and plain serial ports.
Signed-off-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Grant Likely <grant.likely@secretlab.ca>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Easier to follow if platform_data name is pdata.
Signed-off-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Grant Likely <grant.likely@secretlab.ca>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>