In the eMMC 4.51 version of the spec, an EXT_CSD field called
GENERIC_CMD6_TIME[248] was added. This allows cards to specify the maximum
time it may need to move out from its busy state, when a CMD6 command has
been sent.
In cases when the card is compliant to versions < 4.51 of the eMMC spec,
obviously the core needs to use a fall-back value for this timeout, which
currently is set to 10 minutes. This value is completely in the wrong range
and importantly in some cases it causes a card initialization to take more
than 10 minute to complete.
Earlier this scenario was avoided as the mmc core used CMD13 to poll the
card, to find out when it stopped signaling busy. Commit 08573eaf1a
("mmc: mmc: do not use CMD13 to get status after speed mode switch")
changed this behavior.
Instead of reverting that commit, which would cause other issues, let's
instead start by picking a simple solution for the problem, by using a
500ms default generic CMD6 timeout.
The reason for using exactly 500ms, comes from observations that shows it's
quite common for cards to specify 250ms. 500ms is two times that value so
likely it should be enough for most cards.
Cc: <stable@vger.kernel.org> # v4.8+
Fixes: 08573eaf1a ("mmc: mmc: do not use CMD13 to get status after speed
mode switch")
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Stephen Boyd <sboyd@codeaurora.org>
Tested-by: Linus Walleij <linus.walleij@linaro.org>
Per JESD84-B51 P49, Host need to change frequency to <=52MHz
after setting HS_TIMING to 0x1, and host may changes frequency
to <= 200MHz after setting HS_TIMING to 0x3. That means the card
expects the clock rate to increase from the current used f_init
(which is less than 400KHz, but still being less than 52MHz) to
52MHz, otherwise we find some eMMC devices significantly report
failure when sending status.
Reported-by: Xiao Yao <xiaoyao@rock-chips.com>
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Reviewed-by: Douglas Anderson <dianders@chromium.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When introducing hs400es, I didn't notice that we haven't
switched voltage to 1V2 or 1V8 for it. That happens to work
as the first controller claiming to support hs400es, arasan(5.1),
which is designed to only support 1V8. So the voltage is fixed to 1V8.
But it actually is wrong, and will not fit for other host controllers.
Let's fix it.
Fixes: commit 81ac2af657 ("mmc: core: implement enhanced strobe support")
Cc: <stable@vger.kernel.org>
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Reviewed-by: Douglas Anderson <dianders@chromium.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Per spec, block size should always be 512 bytes for dual rate mode,
so any attempts to switch the block size under dual rate mode should
be neglected.
Signed-off-by: Ziyuan Xu <xzy.xu@rock-chips.com>
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
A host controller driver exposes its capability using caps flag
MMC_CAP_CMD_DURING_TFR. A driver with that capability can accept requests
that are marked mrq->cap_cmd_during_tfr = true. Then the driver informs the
upper layers when the command line is available for further commands by
calling mmc_command_done(). Because of that, the driver will not then
automatically send STOP commands, and it is the responsibility of the upper
layer to send a STOP command if it is required.
For requests submitted through the mmc_wait_for_req() interface, the caller
sets mrq->cap_cmd_during_tfr = true which causes mmc_wait_for_req() in fact
not to wait. The caller can then send commands that do not use the data
lines. Finally the caller can wait for the transfer to complete by calling
mmc_wait_for_req_done() which is now exported.
For requests submitted through the mmc_start_req() interface, the caller
again sets mrq->cap_cmd_during_tfr = true, but mmc_start_req() anyway does
not wait. The caller can then send commands that do not use the data
lines. Finally the caller can wait for the transfer to complete in the
normal way i.e. calling mmc_start_req() again.
Irrespective of how a cap_cmd_during_tfr request is started,
mmc_is_req_done() can be called if the upper layer needs to determine if
the request is done. However the appropriate waiting function (either
mmc_wait_for_req_done() or mmc_start_req()) must still be called.
The implementation consists primarily of a new completion
mrq->cmd_completion which notifies when the command line is available for
further commands. That completion is completed by mmc_command_done().
When there is an ongoing data transfer, calls to mmc_wait_for_req() will
automatically wait on that completion, so the caller does not have to do
anything special.
Note, in the case of errors, the driver may call mmc_request_done() without
calling mmc_command_done() because mmc_request_done() always calls
mmc_command_done().
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In most cases the 'card->erase_size' is power of 2, then the round_up/down()
function is more efficient than '%' operation when the 'card->erase_size' is
power of 2.
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Tested-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to clean up the mmc_erase() function and do some optimization
for erase size alignment, factor out the guts of erase size alignment
into mmc_align_erase_size() function.
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Tested-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In cases when the host->max_busy_timeout isn't specified, the calculated
number of maximum discard sectors defaults to UINT_MAX. This may cause a
too long timeout for a discard request.
Avoid this by using a default maximum erase timeout of 60s, used when we
calculate the maximum number of sectors that are allowed to be discarded
per request.
Do note that the minimum number of sectors to be discarded is still at
least one "preferred erase size".
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
When using mmc_io_rw_extended, it's intent to avoid null
pointer of card and invalid func number. But actually it
didn't prevent that as the seg_size already use the card.
Currently the wrapper function sdio_io_rw_ext_helper already
use card before calling mmc_io_rw_extended, so we should move
this check to there. As to the func number, it was token from
'(ocr & 0x70000000) >> 28' which should be enough to guarantee
that it won't be larger than 7. But we should prevent the
caller like wifi drivers modify this value. So let's move this
check into sdio_io_rw_ext_helper either.
Also we remove the BUG_ON for mmc_send_io_op_cond since all
possible paths calling this function are protected by checking
the arguments in advance. After deploying these changes, we
could not see any panic within SDIO API even if func drivers
abuse the SDIO func APIs.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The switch failure message in mmc_select_timing() had been removed
since that is invalid: commit 0400ed0a08 ("mmc: core: remove the
invalid message in mmc_select_timing")
Now, in the case when mmc_select_hs() return error in mmc_select_timing(),
there is nothing to print failure message.
Let's make for mmc_select_hs() print message itself in the failure case.
Signed-off-by: Jungseung Lee <js07.lee@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The SD Status register contains several important fields related to the
SD Card proprietary features.
Those fields may be used by user space applications for vendor specific
usage.
None of those fields are exported today by the driver to user space.
In this patch, we are reading the SD Status register and exporting
(using MMC_DEV_ATTR) the SD Status register to the user space.
Signed-off-by: Uri Yanai <uri.yanai@sandisk.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some devices need a while to boot their firmware after providing clks /
de-asserting resets before they are ready to receive sdio commands.
This commits adds a post-power-on-delay-ms devicetree property to
mmc-pwrseq-simple for use with such devices.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Acked-by: Rob Herring <robh@kernel.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When mmc host HW supports busy signalling (using R1B as response), don't
use the host->max_busy_timeout as the limitation when deciding the max
discard sectors, which we inform the generic BLOCK layer about. Instead,
let's use at least one preferred erase size as the max discard sectors.
In cases when the host controller supports HW busy signalling and the
timeout for the erase operation doesn't exceed the max_busy_timeout, we
keep the R1B response, otherwise we prevent the host from doing HW busy
detection by converting to a R1 response.
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Export DSR register through sysfs same as we did for the CID, CSD and
OCR registers.
Signed-off-by: Bojan Prtvar <prtvar.b@gmail.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The reason for why we expose these to dt is that some of
the controller is unable to send special cmd type due to
the hw limitation.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Registers CID and CSD are already exported through sysfs so let's make
this interface complete by adding missing OCR register.
Signed-off-by: Bojan Prtvar <prtvar.b@gmail.com>
Reviewed-by: Wolfram Sang <wsa@the-dreams.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Host drivers which needs to valdiate for non-supported MMC
commands and returnn error code for such requests.
To improve and simplify the behaviour, let's invent MMC_CAP2_NO_MMC
which these host drivers can set to tell the mmc core to skip sending MMC
commands during card initialization.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There are host drivers which needs to valdiate for non-supported SD
commands and returnn error code for such requests.
To improve and simplify the behaviour, let's invent MMC_CAP2_NO_SD
which these host drivers can set to tell the mmc core to skip sending SD
commands during card initialization.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Certain Hynix eMMC 4.41 cards might get broken when HPI feature is used
and hence this patch disables the HPI feature for such buggy cards.
As some of the other features like BKOPs/Cache/Sanitize are dependent on
HPI feature, those features would also get disabled if HPI is disabled.
Signed-off-by: Pratibhasagar V <pratibha@codeaurora.org>
Signed-off-by: Subhash Jadavani <subhashj@codeaurora.org>
[gdavis: Forward port and cleanup]
Signed-off-by: George G. Davis <george_davis@mentor.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
mmc_select_bus_width() returns bus width (4 or 8) on success or
zero if unsupported. So only change mode if setting the bus width
is successful.
Signed-off-by: Peter Griffin <peter.griffin@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
If available, eMMC stack uses HC_ERASE_GRP_SIZE as the preferred erase
size. As some high capacity eMMC (64MB) reports this size to 512kB, the
discard operations end up taking very long time.
Improve the behaviour by instead calculating the preferred erase size
based on the eMMC size. In this way the discard operations becomes faster.
Signed-off-by: Gwendal Grignou <gwendal@chromium.org>
[Ulf: Updated changelog and improved comment in code]
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To slove the issue which was found on gru board for hs400.
[ 4.616946] sdhci: Secure Digital Host Controller Interface driver
[ 4.623135] sdhci: Copyright(c) Pierre Ossman
[ 4.722575] sdhci-pltfm: SDHCI platform and OF driver helper
[ 4.730962] sdhci-arasan fe330000.sdhci: No vmmc regulator found
[ 4.737444] sdhci-arasan fe330000.sdhci: No vqmmc regulator found
[ 4.774930] mmc0: SDHCI controller on fe330000.sdhci [fe330000.sdhci] using ADMA
[ 4.980295] mmc0: switch to high-speed from hs200 failed, err:-84
[ 4.986487] mmc0: error -84 whilst initialising MMC card
We should change HS400 mode selection timing to meet JEDEC
specification. The JEDEC 5.1 said that change the frequency to <= 52MHZ
after HS_TIMING switch. Refer to section 6.6.2.3 "HS400" timing mode
selection:
Set the "Timing Interface" parameter in the HS_TIMING[185] field of the
Extended CSD register to 0x1 to switch to High Speed mode and then set
the clock frequency to a value not greater than 52MHZ.
Signed-off-by: Ziyuan Xu <xzy.xu@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
with CONFIG_HZ=100, the precision of jiffies is 10ms, and the
generic_cmd6_time of some card is also 10ms. then, may be current
time is only 5ms, but already timed out caused by jiffies precision.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Per JEDEC spec, it is not recommended to use CMD13 to get card status
after speed mode switch. below are two reason about this:
1. CMD13 cannot be guaranteed due to the asynchronous operation.
Therefore it is not recommended to use CMD13 to check busy completion
of the timing change indication.
2. After switch to HS200, CMD13 will get response of 0x800, and even the
busy signal gets de-asserted, the response of CMD13 is aslo 0x800.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some MMC hosts do not support MMC_CAP_WAIT_WHILE_BUSY, but implements the
->card_busy() callback. In such cases, extend __mmc_switch() to use this
method to check card status after switch command.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We introduce HS400 with enhanced strobe function, so we need
to add it for debug show.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Reviewed-by: Douglas Anderson <dianders@chromium.org>
Tested-by: Douglas Anderson <dianders@chromium.org>
Tested-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Controllers use data strobe line to latch data from devices
under hs400 mode, but not for cmd line. So since emmc 5.1, JEDEC
introduces enhanced strobe mode for latching cmd response from
emmc devices to host controllers. This new feature is optional,
so it depends both on device's cap and host's cap to decide
whether to use it or not.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Reviewed-by: Jaehoon Chung <jh80.chung@samsung.com>
Tested-by: Douglas Anderson <dianders@chromium.org>
Tested-by: Jaehoon Chung <jh80.chung@samsung.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch introduce mmc-hs400-enhanced-strobe for platforms
which want to enable enhanced strobe function from DT if the
mmc host controller claims to support enhanced strobe.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Reviewed-by: Douglas Anderson <dianders@chromium.org>
Tested-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When IS_ERR_VALUE was removed from the mmc core code, it was replaced
with a simple not-zero check. This does not work, as the value checked
is the return value for mmc_select_bus_width, which returns the set
bit width on success. This made eMMC modes higher than HS-DDR unusable.
Fix this by checking for a positive return value instead.
Fixes: 287980e49f ("remove lots of IS_ERR_VALUE abuses")
Cc: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Acked-by: Hans de Goede <hdegoede@redhat.com>
Reviewed-by: Krzysztof Kozlowski <k.kozlowski@samsung.com>
Acked-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Tested-by: Marcel Ziswiler <marcel.ziswiler@toradex.com>
Tested-by: Bjorn Andersson <bjorn.andersson@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Most users of IS_ERR_VALUE() in the kernel are wrong, as they
pass an 'int' into a function that takes an 'unsigned long'
argument. This happens to work because the type is sign-extended
on 64-bit architectures before it gets converted into an
unsigned type.
However, anything that passes an 'unsigned short' or 'unsigned int'
argument into IS_ERR_VALUE() is guaranteed to be broken, as are
8-bit integers and types that are wider than 'unsigned long'.
Andrzej Hajda has already fixed a lot of the worst abusers that
were causing actual bugs, but it would be nice to prevent any
users that are not passing 'unsigned long' arguments.
This patch changes all users of IS_ERR_VALUE() that I could find
on 32-bit ARM randconfig builds and x86 allmodconfig. For the
moment, this doesn't change the definition of IS_ERR_VALUE()
because there are probably still architecture specific users
elsewhere.
Almost all the warnings I got are for files that are better off
using 'if (err)' or 'if (err < 0)'.
The only legitimate user I could find that we get a warning for
is the (32-bit only) freescale fman driver, so I did not remove
the IS_ERR_VALUE() there but changed the type to 'unsigned long'.
For 9pfs, I just worked around one user whose calling conventions
are so obscure that I did not dare change the behavior.
I was using this definition for testing:
#define IS_ERR_VALUE(x) ((unsigned long*)NULL == (typeof (x)*)NULL && \
unlikely((unsigned long long)(x) >= (unsigned long long)(typeof(x))-MAX_ERRNO))
which ends up making all 16-bit or wider types work correctly with
the most plausible interpretation of what IS_ERR_VALUE() was supposed
to return according to its users, but also causes a compile-time
warning for any users that do not pass an 'unsigned long' argument.
I suggested this approach earlier this year, but back then we ended
up deciding to just fix the users that are obviously broken. After
the initial warning that caused me to get involved in the discussion
(fs/gfs2/dir.c) showed up again in the mainline kernel, Linus
asked me to send the whole thing again.
[ Updated the 9p parts as per Al Viro - Linus ]
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Cc: Andrzej Hajda <a.hajda@samsung.com>
Cc: Andrew Morton <akpm@linux-foundation.org>
Link: https://lkml.org/lkml/2016/1/7/363
Link: https://lkml.org/lkml/2016/5/27/486
Acked-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org> # For nvmem part
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
008GE0 Toshiba mmc in some Intel Baytrail tablets responds to
MMC_SEND_EXT_CSD in 450-600ms.
This patch will...
() Increase the long read time quirk timeout from 300ms to 600ms. Original
author of that quirk says 300ms was only a guess and that the number
may need to be raised in the future.
() Add this specific MMC to the quirk
Signed-off-by: Matt Gumbel <matthew.k.gumbel@intel.com>
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Re-tuning is not possible when switched to the RPMB
partition. However re-tuning should not be needed
if re-tuning is done immediately before switching,
a small set of operations is done, and then we
immediately switch back to the main partition.
To ensure that re-tuning can't be done for a short
while, add a facility to "pause" re-tuning.
The existing facility to hold / release re-tuning
is used but it also flags re-tuning as needed to cause
re-tuning before the next command (which will be the
switch to RPMB).
We also need to "unpause" in the recovery path, which
is catered for by adding it to mmc_retune_disable().
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some eMMCs set the partition switch timeout too low.
Now typically eMMCs are considered a critical component (e.g. because
they store the root file system) and consequently are expected to be
reliable. Thus we can neglect the use case where eMMCs can't switch
reliably and we might want a lower timeout to facilitate speedy
recovery.
Although we could employ a quirk for the cards that are affected (if
we could identify them all), as described above, there is little
benefit to having a low timeout, so instead simply set a minimum
timeout.
The minimum is set to 300ms somewhat arbitrarily - the examples that
have been seen had a timeout of 10ms but were sometimes taking 60-70ms.
Cc: stable@vger.kernel.org
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
I have two SDIO WLAN cards which specify being SDIO Rev. 1.1 cards but
their FUNCE tuple reports the smaller size of a Rev 1.0 card. So,
enforce 1.0 on these cards to avoid reading the not present registers.
They are not really used anyhow. My cards initialize properly after this
patch.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
mmc_select_hs200() and mmc_select_hs() will keep the timing
as before if switch fails. So it's meaningless to print the
failed switched mode outside based on the current host timing.
Furthermore, the original print is wrong, it should be:
pr_warn("%s: switch to %s failed\n",
mmc_hostname(card->host),
mmc_card_hs(card) ? "high-speed" :
(mmc_card_hs200(card) ? "hs200" : ""));
Since we already have error message in mmc_select_hs200(),
simply remove it outside.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Currently MMC core will keep going if HS200/HS timing switch failed
with -EBADMSG error by the assumption that the old timing is still valid.
However, for mmc_select_hs200 case, the signal voltage may have already
been switched. If the timing switch failed, we should fall back to
the old voltage in case the card is continue run with legacy timing.
If fall back signal voltage failed, we explicitly report an EIO error
to force retry during the next power cycle.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
CMD0 or hardware reset may invalidate the cache, so it needs to be
flushed before reset.
In the case of recovery, we can't expect flushing the cache to work
always, but have a go and ignore errors.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This if-block is going to call mmc_card_set_blockaddr(), so
mmc_card_blockaddr() right before it is redundant.
I am fixing the block comment style while I am here.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
simple-pwrseq and emmc-pwrseq drivers rely on platform_device
structure from of_find_device_by_node(), this works mostly. But, as there
is no driver associated with this devices, cases like default/init pinctrl
setup would never be performed by pwrseq. This becomes problem when the
gpios used in pwrseq require pinctrl setup.
Currently most of the common pinctrl setup is done in
drivers/base/pinctrl.c by pinctrl_bind_pins().
There are two ways to solve this issue on either convert pwrseq drivers
to a proper platform drivers or copy the exact code from
pcintrl_bind_pins(). I prefer converting pwrseq to proper drivers so that
other cases like setting up clks/parents from dt would also be possible.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch adds to_pwrseq_emmc() macro to make the code more readable.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch adds to_pwrseq_simple() macro to make the code more readable.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The eMMC HW reset may be implemented either via the host ops ->hw_reset()
callback or through DT and the eMMC pwrseq. Additionally some eMMC cards
don't support HW reset.
To allow a reset to be done for the different combinations of mmc hosts
and eMMC/MMC cards, let's implement a fallback via trying a regular power
cycle. This improves the mmc block layer retry mechanism of failing I/O
requests.
Signed-off-by: Gwendal Grignou <gwendal@chromium.org>
[Ulf: Rewrote changelog]
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch provides some tracepoints for the lifecycle of a mmc request
from starting to completion to help with performance analysis of MMC
subsystem.
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
PAGE_CACHE_{SIZE,SHIFT,MASK,ALIGN} macros were introduced *long* time
ago with promise that one day it will be possible to implement page
cache with bigger chunks than PAGE_SIZE.
This promise never materialized. And unlikely will.
We have many places where PAGE_CACHE_SIZE assumed to be equal to
PAGE_SIZE. And it's constant source of confusion on whether
PAGE_CACHE_* or PAGE_* constant should be used in a particular case,
especially on the border between fs and mm.
Global switching to PAGE_CACHE_SIZE != PAGE_SIZE would cause to much
breakage to be doable.
Let's stop pretending that pages in page cache are special. They are
not.
The changes are pretty straight-forward:
- <foo> << (PAGE_CACHE_SHIFT - PAGE_SHIFT) -> <foo>;
- <foo> >> (PAGE_CACHE_SHIFT - PAGE_SHIFT) -> <foo>;
- PAGE_CACHE_{SIZE,SHIFT,MASK,ALIGN} -> PAGE_{SIZE,SHIFT,MASK,ALIGN};
- page_cache_get() -> get_page();
- page_cache_release() -> put_page();
This patch contains automated changes generated with coccinelle using
script below. For some reason, coccinelle doesn't patch header files.
I've called spatch for them manually.
The only adjustment after coccinelle is revert of changes to
PAGE_CAHCE_ALIGN definition: we are going to drop it later.
There are few places in the code where coccinelle didn't reach. I'll
fix them manually in a separate patch. Comments and documentation also
will be addressed with the separate patch.
virtual patch
@@
expression E;
@@
- E << (PAGE_CACHE_SHIFT - PAGE_SHIFT)
+ E
@@
expression E;
@@
- E >> (PAGE_CACHE_SHIFT - PAGE_SHIFT)
+ E
@@
@@
- PAGE_CACHE_SHIFT
+ PAGE_SHIFT
@@
@@
- PAGE_CACHE_SIZE
+ PAGE_SIZE
@@
@@
- PAGE_CACHE_MASK
+ PAGE_MASK
@@
expression E;
@@
- PAGE_CACHE_ALIGN(E)
+ PAGE_ALIGN(E)
@@
expression E;
@@
- page_cache_get(E)
+ get_page(E)
@@
expression E;
@@
- page_cache_release(E)
+ put_page(E)
Signed-off-by: Kirill A. Shutemov <kirill.shutemov@linux.intel.com>
Acked-by: Michal Hocko <mhocko@suse.com>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
When initializing sdio card, we get struct mmc_card
from mmc_alloc_card which allocates it by kzalloc. So we
don't need another memset while reading cccr.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When initializing sd or sdio card, we get struct mmc_card
from mmc_alloc_card which allocates it by kzalloc. So we don't
need another memset while decoding cid.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Print the error code when the tuning command fails. This allows the
reason for the failure to be reported, which aids debugging.
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Improve mmc_of_parse_voltage()'s return values so that drivers can tell
whether a voltage-range specification was present, and whether it has
been successfully parsed, or there was an error while parsing.
We return a negative errno when parsing fails, zero if no voltage-range
specification is present, or one if a voltage-range specification is
successfully parsed.
No users need modifying as no users check the return value.
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Each time a driver such as sdhci-esdhc-imx is probed, we get a info
printk complaining that the DT voltage-ranges property has not been
specified.
However, the DT binding specifically says that the voltage-ranges
property is optional. That means we should not be complaining that
DT hasn't specified this property: by indicating that it's optional,
it is valid not to have the property in DT.
Silence the warning if the property is missing.
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>