mirror of https://gitee.com/openkylin/linux.git
65e4345c8e
The LIS3LV02 has a special bit that need to be set to get the
read values left aligned. Before this patch we get gibberish
like this:
iio_generic_buffer -a -c10 -n lis3lv02dl_accel
(...)
0.000000 -0.010042 -0.642688 19155832931907
0.000000 -0.010042 -0.642688 19155858751073
Which is because we read a raw value for 1g as 64 which is
the nominal 1024 for 1g shifted 4 bits to the left by being
right-aligned rather than left aligned.
Since all other sensors are left aligned, add some code to
set the special DAS (data alignment setting) bit to 1 so that
the right value is now read like this:
iio_generic_buffer -a -c10 -n lis3lv02dl_accel
(...)
0.000000 -0.147095 -10.120135 24761614364956
-0.029419 -0.176514 -10.120135 24761631624540
The scaling was weird as well: we have a gain of 1000 for 1g
and 3000 for 6g. I don't even remember how I came up with the
old values but they are wrong.
Fixes:
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.. | ||
cros_ec_sensors | ||
hid-sensors | ||
ms_sensors | ||
ssp_sensors | ||
st_sensors | ||
Kconfig | ||
Makefile |