mirror of https://gitee.com/openkylin/linux.git
869c6a3ede
The timing calculation is rather bogus and gives extremely wrong results for higher frequencies (on an i.MX28). E.g. instead of 400 kHz I measured 770 kHz. Implement a calculation that adheres to the I2C spec and gives exact results for I2C frequencies from 12.56 kHz to 960 kHz. Also the bus_free and leadin parameters are programmed according to the I2C spec for standard and fast mode. This was tested on a Ka-Ro TX28 module with a DS1339, TSC2007, PCA9554 and SGTL5000 client. Signed-off-by: Lothar Waßmann <LW@KARO-electronics.de> Acked-by: Marek Vasut <marex@denx.de> [wsa: patch fixes whitespace issue, too] Signed-off-by: Wolfram Sang <wsa@the-dreams.de> |
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.. | ||
algos | ||
busses | ||
muxes | ||
Kconfig | ||
Makefile | ||
i2c-boardinfo.c | ||
i2c-core.c | ||
i2c-core.h | ||
i2c-dev.c | ||
i2c-mux.c | ||
i2c-smbus.c | ||
i2c-stub.c |