rndis_wlan devices freeze after running usbnet_stop several times. It appears
that firmware freezes in state where it does not respond to any RNDIS commands
and device have to be physically unplugged/replugged. This patch lets
minidrivers to disable unlink_urbs on usbnet_stop through new info flag.
Signed-off-by: Jussi Kivilinna <jussi.kivilinna@mbnet.fi>
Cc: David Brownell <dbrownell@users.sourceforge.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Even with the split into iwlcore/agn/3945 not all symbols
that cross file boundaries are needed in other modules, a
few are only used within iwlcore, for example.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
The mac80211 workqueue exists to enable mac80211 and drivers
to queue their own work on a single threaded workqueue. mac80211
takes care to flush the workqueue during suspend but we never
really had requirements on drivers for how they should use
the workqueue in consideration for suspend.
We extend mac80211 to document how the mac80211 workqueue should
be used, how it should not be used and finally move raw access to
the workqueue to mac80211 only. Drivers and mac80211 use helpers
to queue work onto the mac80211 workqueue:
* ieee80211_queue_work()
* ieee80211_queue_delayed_work()
These helpers will now warn if mac80211 already completed its
suspend cycle and someone is trying to queue work. mac80211
flushes the mac80211 workqueue prior to suspend a few times,
but we haven't taken the care to ensure drivers won't add more
work after suspend. To help with this we add a warning when
someone tries to add work and mac80211 already completed the
suspend cycle.
Drivers should ensure they cancel any work or delayed work
in the mac80211 stop() callback.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
This driver only uses the mac80211 workqueue and mac80211 requires us to
cancel all work at driver stop. Since we now have the cancels in the right
places at stop() we really don't need to flush the mac80211 workqueue so
remove it.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Acked-by: Kalle Valo <kalle.valo@iki.fi>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We need to process tx descriptors for all queues (currently main tx
queue and cabq) which may have triggered the TX completion interrupt.
Otherwise, the queues can get stuck after sending a few frames.
Signed-off-by: Bob Copeland <me@bobcopeland.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Cc: Christian Lamparter <chunkeey@web.de>
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
As shown in http://thread.gmane.org/gmane.linux.kernel.wireless.general/36497,
mac80211 has a bug that allows a call to the TX routine after the queues have
been stopped. This situation will only occur under extreme stress. Although
b43 does not crash when this condition occurs, it does generate a WARN_ON and
also logs a queue overrun message. This patch recognizes b43 is not at fault
and logs a message only when the most verbose debugging mode is enabled. In
the unlikely event that the queue is not stopped when the DMA queue becomes
full, then a warning is issued.
During testing of this patch with one output stream running repeated tcpperf
writes and a second running a flood ping, this routine was entered with
the DMA ring stopped about once per hour. The condition where the DMA queue is
full but the ring has not been stopped has never been seen by me.
Signed-off-by: Larry Finger <Larry.Finger@lwfinger.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Previously, we would store the operating mode at interface up time,
but only update the PCU registers when the next reset happened.
The result is that if beacon configuration (ops->bss_info_changed)
happens before ops->config, we will program the wrong things into
the timer registers. Consequently, beacons won't work in AP mode
until after a reset (channel change, scan etc.).
This is fragile anyway so just program the opmode as soon as
mac80211 gives it to us.
Signed-off-by: Bob Copeland <me@bobcopeland.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Monotonicity of packet error rate should be kept when moving
from one phy to another (legacy to ht, ht single stream to dual,
etc). Current code skips updating per for other phys.
Signed-off-by: Vasanthakumar Thiagarajan <vasanth@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Now the lowest rate in 11na ht40 mode is 13.5Mbps this shortens the
range when compared to 11na ht20 mode where the lowest rate is 6.5Mbps.
To improve the range, make 6.5Mbps as the lowest rate in 11na ht40 mode,
this improves the range by approximately 2dB. 11ng ht40 does not have
this issue as it also has basic rates (1, 2, 5.5 and 11).
Signed-off-by: Vasanthakumar Thiagarajan <vasanth@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
When only rt2400pci or rt2500pci is compiled without any of the other
rt2x00 modules, then CONFIG_RT2X00_LIB_CRYPTO will not be enabled.
However rt2x00mac_set_tim() implemented within #ifdef CONFIG_RT2X00_LIB_CRYPTO
statements while the declaration is placed outside the definition. This results in linking
errors as reporte by Ken.
rt2x00_set_tim() has nothing to do with crypto, and thus should be moved outside
of the #ifdef statements.
Signed-off-by: Ivo van Doorn <IvDoorn@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
These drivers have been around for a while, if there are issues
they should be reported. rt2800usb is still a bit flaky though.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Acked-by: Ivo van Doorn <IvDoorn@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
This should make it very clear which are pre-802.11 or not
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Make atheros wireless drivers visible when you select
"Atheros wirless drivers". Adds links to ath.ko page,
and Atheros drivers page on the wiki.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
The ath.ko module itself depends on cfg80211
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
cancel_delayed_work_sync() and cancel_work_sync() are already being
used therefore already waiting for all pending work by the driver
to have been completed, no need to flush the mac80211 workqueue.
Cc: Christian Lamparter <chunkeey@web.de>
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
This should fix suspend as mac80211 expects all work queued
to the mac80211 workqueue to be canceled at driver stop().
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Acked-by: Kalle Valo <kalle.valo@iki.fi>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We weren't ever cancelling this.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Acked-by: Kalle Valo <kalle.valo@iki.fi>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We should be cancelling our work at the stop callback since
we are borrowing the mac80211 workqueue for our work. As it
stands mac80211 expects this for suspend purposes.
The ath9k specific virtual wiphy stuff need only be
cancelled only when the we have no secondary virtual wiphys.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We do this as we'll be moving the cancel elsewhere later.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
ath9k uses the mac80211 workqueue for 4 different types of work:
* Led blink work
* TX hang monitoring work
* internal wiphy schedular work
* channel change work done for internal wiphy schedular
Since the internal wiphy schedular can end up kicking off some
channel channel change work we should first cancel the wiphy
schedular work and then the channel change work.
The TX hang work can be cancelled second since we're going down
anyway.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
The eeprom read & write commands currently check the E2P_CMD_LOADED_ bit is
set before allowing any operations. This prevents any reading or writing
unless a correctly programmed EEPROM is installed.
This patch removes the check, so it is possible to program blank EEPROMS
via ethtool.
Signed-off-by: Steve Glendinning <steve.glendinning@smsc.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The kernel.h macro DIV_ROUND_CLOSEST performs the computation (x + d/2)/d
but is perhaps more readable.
The semantic patch that makes this change is as follows:
(http://www.emn.fr/x-info/coccinelle/)
// <smpl>
@haskernel@
@@
#include <linux/kernel.h>
@depends on haskernel@
expression x,__divisor;
@@
- (((x) + ((__divisor) / 2)) / (__divisor))
+ DIV_ROUND_CLOSEST(x,__divisor)
// </smpl>
Signed-off-by: Julia Lawall <julia@diku.dk>
Signed-off-by: David S. Miller <davem@davemloft.net>
Modify control register settings to accommodate the bridge's max read
requset size.
Signed-off-by: Divy Le Ray <divy@chelsio.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Fix a cut'n paste error in the AEL2020 twinax EDC file name
Signed-off-by: Divy Le Ray <divy@chelsio.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for vxge.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for s2io.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for qlge.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for ixgb.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for igbvf.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for bnx2x.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for bnx2.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for atl1e.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
PCI drivers that implement the struct pci_error_handlers' error_detected
callback should return PCI_ERS_RESULT_DISCONNECT if the state passed in is
pci_channel_io_perm_failure. This patch fixes the issue for atl1c.
Signed-off-by: Dean Nelson <dnelson@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When the driver loads the POST stage of the card is expected to be
POST_STAGE_ARMFW_RDY.
Signed-off-by: Sathya Perla <sathyap@serverengines.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
be_mbox_db_ring() has been changed to be_mbox_notify() (to be consistent with
be_mcc_notify()) and struct be_mcc_cq_entry changed to be_mcc_compl
to be consistent with rx/tx_compl.
Signed-off-by: Sathya Perla <sathyap@serverengines.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
pci function is available as PCI_FUNC(pdev->devfn); no need for a
separate field.
Signed-off-by: Sathya Perla <sathyap@serverengines.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Currently only the be_ctrl_info struct ptr (instead of adapter) is
passed to all the routines in be_cmds.c. Instead pass be_adapter
ptr to allow access to all its fields. Merge the contents of struct be_ctrl_info
into be_adapter. The resulting code is simpler.
Signed-off-by: Sathya Perla <sathyap@serverengines.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When a user disables interrupt throttling with ethtool on 82599 devices,
the interrupt timer may not be re-enabled if hardware RSC is running. The
RSC completions in hardware don't complete before the next ITR event tries
to fire, so the ITR timer never gets re-armed. This patch increases the
amount of time between interrupts when throttling is disabled (rx-usecs =
0) when the hardware RSC deature is enabled.
Signed-off-by: Peter P Waskiewicz Jr <peter.p.waskiewicz.jr@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
A second set of feature flag bits was added, and the hardware RSC engine
flags were moved there. However, the code itself didn't make the move
completely to use the new bitmap.
Signed-off-by: Peter P Waskiewicz Jr <peter.p.waskiewicz.jr@intel.com>
Acked-by: Mallikarjuna R Chilakala <mallikarjuna.chilakala@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Our ndo_poll_controller callback is broken for anything but non-multiqueue
setups. This fixes that issue.
Signed-off-by: Peter P Waskiewicz Jr <peter.p.waskiewicz.jr@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Parameter order for using mk_ic_value(count, time) was reversed,
the patch fixes this.
Signed-off-by: Jiajun Wu <b06378@freescale.com>
Signed-off-by: Li Yang <leoli@freescale.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
If a socket is hashed in last slot of pppoe hash table (PPPOE_HASH_SIZE-1)
we report it many times (up to filling seq buffer)
(Only the last socket of last slot)
Signed-off-by: Eric Dumazet <eric.dumazet@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
start_code is 69 words, but the code always writes a multiple of 16 words,
so the last 11 words written are outside the array.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
if dev_alloc_skb() fails on the first iteration, a write to
cp->rx_ring[-1] occurs.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In some cases with 57711E, depending on the functions unload sequence, other
functions MAC address could have been used to wake the system as well. Make sure
to block all but the current function if WoL is required by changing the mode
to single function WoL.
Signed-off-by: Eilon Greenstein <eilong@broadcom.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Self test used to play with the management FIFO possibly while management was
running...
Signed-off-by: Eilon Greenstein <eilong@broadcom.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Due to lack of configuration, if the BMC configures the chip to pass all
broadcast/multicast traffic to it, the host will not receive it. On top of
fixing it, also make sure that in promiscuous mode, the host will receive the
management traffic as well.
Signed-off-by: Eilon Greenstein <eilong@broadcom.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Wrap dest IP hashing code with #ifdef CONFIG_INET,
this feature makes no sense without INET, but other
driver can still work.
Signed-off-by: Dhananjay Phadke <dhananjay@netxen.com>
Acked-by: Randy Dunlap <randy.dunlap@oracle.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Add debugfs file to enable/disable HT40(40MHz) channel support.
By default, 40MHz is supported if AP can support the function.
By echo "1" to "disable_ht40" file, iwlwifi driver will disable the
40MHz support and only allow 20MHz channel.
Because the information exchange happen during association time,
so enable/disable ht40 channel only can be performed when it is not
associated with AP.
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Our version goes by the kernel release.
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Finally! This is what you've all been waiting for!
This patch makes cfg80211 take care of wext emulation
_completely_ by itself, drivers that don't need things
cfg80211 doesn't do yet don't even need to be aware of
wireless extensions.
This means we can also clean up mac80211's and iwm's
Kconfig and make it possible to build them w/o wext
now!
RIP wext.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Since we now have handlers IWESSID for all modes, we can
combine them into one.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Since we now have IWAP handlers for all modes, we can
combine them into one.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Until now we implemented iwfreq for managed mode, we
needed to keep the implementations separate, but now
that we have all versions implemented we can combine
them and export just one handler.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We are using setpower routines regardless of the current power mode.
Don't bother the hardware, if it is not necessary.
Changes-licensed-under: ISC
Signed-off-by: Gabor Juhos <juhosg@openwrt.org>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
There is a small window where the mac80211 changes the IEEE80211_CONF_PS
flag, and then informs the driver about the change. We have a race
condition if we are checking the flag in the same time. Avoid it by
introducing a local variable, and using that instead of checking the
IEEE80211_CONF_PS flag directly.
This fix the problem reported by Luis:
http://article.gmane.org/gmane.linux.kernel.wireless.general/34363
Changes-licensed-under: ISC
Signed-off-by: Gabor Juhos <juhosg@openwrt.org>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Fix this build error when CONFIG_AR9170_LEDS is not set
drivers/net/wireless/ath/ar9170/main.c:1296: error: 'struct ar9170' has
no member named 'led_work'
Signed-off-by: Alexander Beregalov <a.beregalov@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
C [M] drivers/net/wireless/iwlwifi/iwl-core.o
drivers/net/wireless/iwlwifi/iwl-core.c:1341: warning:
‘iwl_dump_nic_error_log’ defined but not used
Reported-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Commit "iwlwifi: Handle new firmware file with ucode build number
in header" introduced new ucode header parsing routines, but
neglected to initialize these routines for 1000. The system thus goes
into infinite loop trying to load ucode, failing every time with a null
pointer exception as it tries to parse the header.
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Acked-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Several arrays were read before checking whether the index was within
bounds. ARRAY_SIZE() should be used to determine the size of arrays.
rates->rates has an arraysize of 1, so calling get_common_rates()
with a rates_size of MAX_RATES (14) was causing reads out of bounds.
tmp_size can increment at most to (ARRAY_SIZE(lbs_bg_rates) - 1) *
(*rates_size - 1), so that should be the number of elements of tmp[].
A goto can be eliminated: ret was already set upon its declaration.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
reads bss->rates[j] before checking bounds of index, and should use
ARRAY_SIZE to determine the size of the array.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Acked-by: Holger Schurig <hs4233@mail.mn-solutions.de>
Acked-by: Dan Williams <dcbw@redhat.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
IWLWIFI_LEDS option should certainly have help comment, and should
default to y.
Signed-off-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Fix incorrect name for HT MPDU Density.
default set to 4 uSec
Reported-by: Sujith <Sujith.Manoharan@atheros.com>
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
This data is more useful to debugging that the receive
buffer contents.
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
No existing callbacks use anything other than the return
value 1, which means that the caller should free the
reply skb, so it seems safer in terms of not introducing
memory leaks to simply remove the return value and let
the caller always free the skb.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
The current command sending in iwlwifi is a bit of a mess:
1) there is a struct, iwl_cmd, that contains both driver
and device data in a single packed structure -- this
is very confusing
2) the on-stack data and the command metadata share a
structure by embedding the latter in the former, which
is also rather confusing because it leads to weird
unions and similarly odd constructs
3) each txq always has enough space for 256 commands,
even if only 32 end up being used
This patch fixes these things:
1) rename iwl_cmd to iwl_device_cmd and keep track of
command metadata and device command separately, in
two arrays in each tx queue
2) remove the 'meta' member from iwl_host_cmd and only
put in the required members
3) allocate the cmd/meta arrays separately instead of
embedding them into the txq structure
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Add debugfs function to display current thermal throttling status for
both Legacy and Advance Thermal Throttling Management
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Part 2 of Thermal Throttling Management -
Thermal Throttling feature is used to put NIC into low power state when
driver detect the Radio temperature reach pre-defined threshold
Two Thermal Throttling Management Methods; this patch introduce the
Advance Thermal Throttling:
TI-0: system power index, no tx/rx restriction, HT enabled
TI-1: power index 5, 1 spatial stream Tx, multiple spatial stream Rx, HT
enabled
TI-2: power index 5: 1 spatial stream Tx, 1 spatial stream Rx, HT
disabled
TI-CT-KILL: power index 5, no Tx, no Rx, HT disabled
For advance Thermal Throttling, CT_KILL_ENTER threshold and CT_KILL_EXIT
threshold are different; uCode will not stay awake until reach
CT_KILL_EXIT threshold.
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Part 1 of Thermal Throttling Management -
Thermal Throttling feature is used to put NIC into low power state when
driver detect the Radio temperature reach pre-defined threshold
Two Thermal Throttling Management Methods; this patch introduce the
Legacy Thermal Management:
IWL_TI_0: normal temperature, system power state
IWL_TI_1: high temperature detect, low power state
IWL_TI_2: higher temperature detected, lower power state
IWL_TI_CT_KILL: critical temperature detected, lowest power state
Once get into CT_KILL state, uCode go into sleep, driver will stop all
the active queues, then move to IWL_TI_CT_KILL state; also set up 5
seconds timer to toggle CSR flag, uCode wake up upon CSR flag change,
then measure the temperature.
If temperature is above CT_KILL exit threshold, uCode go backto sleep;
if temperature is below CT_KILL exit threshold, uCode send Card State
Notification response with appropriate CT_KILL status flag, and uCode
remain awake, Driver receive Card State Notification Response and update
the card temperature to the CT_KILL exit threshold.
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
If advance thermal throttling is used the driver need to pass both
"enter" and "exit" temperature to uCode.
Using different critical temperature threshold for legacy and advance
thermal throttling management based on the type of thermal throttling
method is used except 1000.
For 1000, it use advance thermal throttling critical temperature
threshold, but with legacy thermal management implementation until ucode
has the necessary implementations in place.
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
When performing rate scaling, if detected that the new rate
index is invalid, clear the search_better_tbl flag
so it will not be stuck in the loop.
Since the search table is already set up in uCode,
we need to empty out the the search table;
revert back to the "active" rate and throughput info.
Also pass the "active" table setup to uCode to make
sure the rate scale is functioning correctly.
Signed-off-by: Wey-Yi Guy <wey-yi.w.guy@intel.com>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
When a station queries us for a PS-poll response, we wrongly
queue the frame on the virtual interface's queue rather than
the pending queue.
Additionally, fix a race condition where we could potentially
send multiple frames to the sleeping station due to using a
station flag rather than a packet flag. When converting to a
packet flag, we can also convert p54 and remove the filter
clearing we added for it.
(Also remove a now dead function)
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Reported-by: Bob Copeland <me@bobcopeland.com>
Tested-by: Bob Copeland <me@bobcopeland.com>
Cc: Christian Lamparter <chunkeey@web.de>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Cleanup aggregation start/stop function interfaces.
Signed-off-by: Sujith <Sujith.Manoharan@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
TH gets 5 GHz.
Cc: David Quan <david.quan@atheros.com>
Cc: Michael Green <michael.green@atheros.com>
Signed-off-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
rt2x00dev->default_ant should be initialized once by the driver,
and should not be changed afterwards. Because rt2x00lib_config_antenna()
was using a reference to the struct antenna_setup it actually had the oppurtunity
to change the default antenna setting and it actually did that during the validation.
Instead of passing a pointer to antenna_setup the entire structure should be copied.
Signed-off-by: Lars Ericsson <Lars_Ericsson@telia.com>
Signed-off-by: Ivo van Doorn <IvDoorn@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
tid is bounded (above) by the size of default_tid_to_tx_fifo (17 elements), but
the size of priv->stations[].tid[] is MAX_TID_COUNT (9) elements.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
Incorrect limits leads to reads outside array bounds.
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Acked-by: Luis R. Rodriguez <lrodriguez@atheros.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
SSID_rid has space for only 3 ssids.
txPowerLevels[i] is read before the bounds check for i
Signed-off-by: Roel Kluin <roel.kluin@gmail.com>
Acked-by: Dan Williams <dcbw@redhat.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
iwm_wdev_alloc() returns an ERR_PTR on failure and not null. It also
prints its own dev_err() message so I removed that as well.
Compile tested only. Sorry.
Found by smatch (http://repo.or.cz/w/smatch.git).
Signed-off-by: Dan Carpenter <error27@gmail.com>
Acked-by: Zhu Yi <yi.zhu@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
We need to provide a reasonable minimum that will result in a
working setup if used. Set minimum to be 10 to provide for
4 standard TX queues + 1 command queue + 2 (unused) HCCA queues +
4 HT queues (one per AC).
We allow the user to change the number of queues used via a module
parameter and use this minimum value to check if it is valid. Without
this patch a user can select a value for the number of queues that
will result in a failing setup.
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Reviewed-by: Tomas Winkler <tomas.winkler@intel.com>
Acked-by: Tomas Winkler <tomas.winkler@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
I had a problem on 4965 hardware (well, probably other hardware too,
but others don't survive my stress testing right now, unfortunately)
where the driver was sending invalid commands to the device, but no
such thing could be seen from the driver's point of view. I could
reproduce this fairly easily by sending multiple TCP streams with
iperf on different TIDs, though sometimes a single iperf stream was
sufficient. It even happened with a single core, but I have forced
preemption turned on.
The culprit was a queue overrun, where we advanced the queue's write
pointer over the read pointer. After careful analysis I've come to
the conclusion that the cause is a race condition between iwlwifi
and mac80211.
mac80211, of course, checks whether the queue is stopped, before
transmitting a frame. This effectively looks like this:
lock(queues)
if (stopped(queue)) {
unlock(queues)
return busy;
}
unlock(queues)
... <-- this place will be important
there is some more code here
drv_tx(frame)
The driver, on the other hand, can stop and start queues, which does
lock(queues)
mark_running/stopped(queue)
unlock(queues)
[if marked running: wake up tasklet to send pending frames]
Now, however, once the driver starts the queue, mac80211 can see that
and end up at the marked place above, at which point for some reason the
driver seems to stop the queue again (I don't understand that) and then
we end up transmitting while the queue is actually full.
Now, this shouldn't actually matter much, but for some reason I've seen
it happen multiple times in a row and the queue actually overflows, at
which point the queue bites itself in the tail and things go completely
wrong.
This patch fixes this by just dropping the packet should this have
happened, and making the lock in iwlwifi cover everything so iwlwifi
can't race against itself (dropping the lock there might make it more
likely, but it did seem to happen without that too).
Since we can't hold the lock across drv_tx() above, I see no way to fix
this in mac80211, but I also don't understand why I haven't seen this
before -- maybe I just never stress tested it this badly.
With this patch, the device has survived many minutes of simultanously
sending two iperf streams on different TIDs with combined throughput
of about 60 Mbps.
Signed-off-by: Johannes Berg <johannes@sipsolutions.net>
Signed-off-by: Reinette Chatre <reinette.chatre@intel.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
res has already been tested. It seems that this test should be on the
recently returned value mmio.
A simplified version of the semantic match that finds this problem is as
follows: (http://www.emn.fr/x-info/coccinelle/)
// <smpl>
@r exists@
local idexpression x;
expression E;
@@
if (x == NULL || ...) { ... when forall
return ...; }
... when != \(x=E\|x--\|x++\|--x\|++x\|x-=E\|x+=E\|x|=E\|x&=E\|&x\)
(
*x == NULL
|
*x != NULL
)
// </smpl>
Signed-off-by: Julia Lawall <julia@diku.dk>
Signed-off-by: David S. Miller <davem@davemloft.net>